Pilot Testing of Mercury Oxidation Catalysts for Upstream of Wet FGD …...

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Pilot Testing of Oxidation Catalysts for Enhanced Mercury Control by Wet FGD Gary Blythe URS Corporation Austin, TX

Transcript of Pilot Testing of Mercury Oxidation Catalysts for Upstream of Wet FGD …...

Pilot Testing of Oxidation Catalysts for Enhanced Mercury

Control by Wet FGD

Gary Blythe

URS Corporation

Austin, TX

Hg Control Technology Concept

• Catalytic oxidation of Hg0 in flue gas to increase overall Hg removal across wet FGD systems

• Initial development is focused on PRB and lignite fuels - higher Hg0

percentages in flue gas• Catalyst to be installed at ESP outlet

Illustration of Process Concept

Wet FGD System (SO2/Hg Removal)

ESP

Mercury Oxidation Catalyst

Process Development Background

• Initial concept development funded by EPRI (early 1990s)

• Further development in DOE NETL/ EPRI co-funded MegaPRDA Project– Lab screening of candidate catalyst

materials– 6-month sand bed tests with promising

catalysts at three coal fired sites– Completed in 2001

Current Project

• Conduct pilot-scale tests of honeycomb Hg0

oxidation catalysts at two sites– 4 catalysts tested in parallel (~2000 acfm each)– 14-months automated operation at each site– Monthly activity measurements with Hg SCEM– Ontario Hydro relative accuracy tests at beginning,

middle, end of test periods

• DOE/NETL, EPRI, utility co-funded

• Host stations include ND lignite (GRE’s Coal Creek), PRB fuels (CPS’s Spruce)

Catalyst Types Tested

• Metal-based– Palladium (Pd #1) - both sites– Ti/V from Argillon (SCR) - both sites– Gold (Au) - Spruce only

• Carbon-based– Experimental activated carbon (C #6) - both sites

• Fly-ash-based– Subbituminous coal ash from one particular plant

(SBA #5) - CCS only

Pilot Unit Concept

From ESPor Baghouse

DPI

DataLogger

InducedDraft Fan

Mercury OxidationCatalyst

FIC

HgHg

TE

TI

To FGD

Pilot Testing Status

• First pilot unit started up at Coal Creek in October 02– 2 of 4 catalysts installed (Pd #1 and SCR)– Delivery of other two catalysts delayed due to

developmental nature of their production

• 3rd catalyst (SBA #5) installed December 02

• 4th catalyst (C #6) installed June 03

• Second pilot unit to start up at Spruce Plant later this month

Pilot Unit at Coal Creek Station

Catalyst Dimensions for Pilot Unit

Catalyst

Cells perin.2

(cpsi)

CrossSection(in. x in.)

Length(in.)

AreaVelocity(sft/hr)

Pd #1 64 30 x 30 9 49

C #6 80* 36 x 36 9 27

SBA #5 80* 36 x 36 9 27

SCR 46 35.4 x 35.4 19.7 14***Die sized for 64 cpsi, cores shrank during drying**1500 acfm, other catalysts operate at 2000 acfm

Photo of Argillon GmbH SCR Catalyst Module

One of Three SBA #5 Catalyst Modules

Close-up of One SBA #5 Block

Initial CCS Pilot Activity ResultsOct. 02 field results vs. lab predictions

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Pd #1 - CCSPd #1 - PredictedSCR - CCSSCR - Predicted

December 02 Results

• Measured activity of Pd #1 and SCR catalysts after ~2 months– Both catalysts showed activity loss

• Pressure drop across both catalysts had substantially increased

• Suspected fly ash buildup in horizontal catalysts

January 03 Results

• Measured performance to see if trend for loss of activity continued– Activity slightly improved since December– Pressure drop indicated continued ash buildup

• Opened catalyst boxes, confirmed fly ash buildup

• Used plant air and vacuum to clean

• Re-measured performance

Surface of Pd #1 Catalyst Prior to Cleaning

Surface of Pd #1 Catalyst after Cleaning

Catalyst Activity Results

Hg0 Oxidation across Catalyst (%)Catalyst(Flow Rate,acfm) October December January

January(aftercleaning)

Pd #1 (2000) 93 53 58 91SCR (1500 ) 67 28 37 61SBA #5(2000)

na* na* 59 75

Efforts to Resolve Ash Buildup

• Identified sonic horns as a likely mechanism to limit fly ash buildup– Commonly used to clean SCR catalysts

• Tested horn (Analytec 17”) on Pd #1 catalyst chamber– Installed perpendicular to chamber inlet

transition duct– Appeared effective in 2 mos. operation– Installed on other chambers June 03

Sonic Horn Installation on Pilot Unit

Sonic Horn Location

Catalyst Pressure Drop thru 5/27 (shows sonic horn effect on Pd #1 catalyst)

Pd #1

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Catalyst Activity Trends over First 8 Months at Coal Creek

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C #6 (initial)

Cleaned Catalyst

Installed Sonic Horn Cleaned

Catalyst (removed light dusting)

Catalyst Activity Trends over First 8 Months at Coal Creek

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1-Oct 1-Dec 31-Jan 2-Apr 2-Jun 2-Aug

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SCR

SBA #5

Cleaned Catalysts

Installed Sonic Horn,

Cleaned Catalysts

Catalyst Pressure Drop since 6/5 (sonic horns in all 4 compartments)

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SBA #5SCRC #6Pd #1

Flue Gas Characterization Results - Other Species

• Ontario Hydro results show good agreement with EPRI Hg SCEM

• Controlled Condensation results showed no oxidation of SO2 across catalysts– Catalyst inlet and outlet SO3 ~0.1 ppmv

• Little or no oxidation of NO across catalysts– Inlet and outlet NO, total NOX values agree within 10

ppm (precision level of technique)

• M26a showed no change in HCl (~1 ppm) or HF (~6 ppm) across catalysts

Lab Testing

• 1 to 2 l/min testing of catalyst cores in simulated flue gas (SO2, HCl, NOX, etc.)

• Tested TVA’s patented gold catalyst in honeycomb form, varied gold loadings– Activity compares favorably with Pd #1– May be effective at lower wash coat loading on

alumina than Pd #1– Selected as 4th catalyst for Spruce (SBA #5 fly

ash not a likely commercial catalyst source)

• Tested other catalyst materials at Spruce conditions

Results of Spruce Laboratory Simulations

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% H

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Pd #1, 3x, 1" lengthSBA #5, 0.5" lengthAu, 1x, 1" length (preliminary)Au 1x, 1"length, repeatSCR, 1"lengthC #6, 1"length

Catalyst Selection for Spruce Pilot

• Pd #1 and C #6 selected based on high activity at CCS

• Au selected based on positive lab results– Need field results to compare activity, life to Pd #1

• Will test SCR catalyst in spite of activity loss at CCS– Loss could be site specific based on previous

PRDA sand bed results with other catalysts

• All catalysts re-ordered at current pitch (Au the same as Pd)

Current Schedule

• Continue SCEM measurement trips to Coal Creek through early 04 – Conduct 3rd set of Ontario Hydro SCEM

relative accuracy tests ~March 04

• Start up 2nd pilot unit at Spruce later in August– Initial shake-down operation w/o catalysts– Expect Pd and Au catalysts by end of August– SCR and C #6 catalysts late September

Proposed Follow-on Project• Proposal submitted in NETL large-scale Hg control

testing solicitation

• Would use existing pilot units to test Hg oxidation catalysts at 2 new sites starting Spring 04– TXU’s Monticello Station (Tx lignite/PRB blend)– Duke Energy’s Marshall Station (low S Eastern bit.)

• Proposed effort would integrate new wet FGD pilot unit downstream of oxidation catalysts– 2000 acfm flow rate to match catalysts– Would test LSFO vs. Mg-lime chemistries

Summary

• Pilot tests results verify previous sand-bed results for the ability to catalytically oxidize Hg0 in flue gases– Honeycomb catalysts have achieved over 90%

oxidation of Hg0 in ND lignite flue gas

• On-line cleaning (sonic horns) needed to prevent fly ash buildup in horizontal gas flow catalysts

• Continued testing will establish catalyst life for two coal types