Lessons Learned from an Unusual Hydrogen Reformer Furnace ... 2005... · 4 Securing Canada’s...
Transcript of Lessons Learned from an Unusual Hydrogen Reformer Furnace ... 2005... · 4 Securing Canada’s...
1Securing Canada’s Energy Future
55th Canadian Chemical Engineering ConferenceProcess Safety and Loss Management
Lessons Learned from an Unusual Hydrogen Reformer
Furnace FailureT. M.Rogers
Syncrude Canada Limited
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QUICK FACTSSyncrude Canada Ltd is a joint venture partnership which converts Athabasca Oilsands into a Light Sweet Blend Crude OilThe facility is an integrated mining, extraction and upgrading operation supported by a common power utilityCurrent capacity is 250,000 barrels/day of final product which is shipped via pipeline to southern marketsThe Upgrading plant is similar to an oil refinery with two separate operating trains each including a crude unit, fluid coker and hydrotreaters
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QUICK FACTSWithin the Upgrading plant 300 MSCFD of hydrogen in three steam/ methane reformers is producedThe incident occurred in the reformer furnace of unit 3
Furnace FactsHydrogen output 81 MSCFD built in 1987 and operational in 1988The radiant section of the furnace contains eight (8) parallel rows of. Each row contains forty-six (46) tubes for a total of 368 tubes composed of spun cast HP-45 Niobium Modified Alloy with a design wall tube temperature of 935oC. Each tube has a 4” ID by 39’10”
108 burners arranged in 9 rows
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SSH
MFPH
Convection Box 1SG-1A
FPH
SG-1B
Aux Burners
SG-2
SG-3
Convection Box 2
BFW
A B C D E F G H I
1 2 3 4 5 6 7 8
Flue Gas
General Furnace Arrangement
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General Tube Arrangement
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SUMMARYTHE INCIDENT
At 22:39 Sunday January 30, 2005 a rapid sudden high energy pressure impulse occurred within several radiant tubes in the unit 3 reformer furnaceThe furnace was in a startup mode on steam without hydrocarbon feedThis impulse caused the simultaneous rupture of 5 tubes with sufficient force to eject portions of the tubes out through the roof of the furnace
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SUMMARY…41 more tubes were destroyed as a result of impacts by tube segments and the subsequent shock waveAll of the flue gas tunnels suffered extensive damageFire box sustained impact damage from shrapnel hitsOne Operator sustained serious injuries when he was hit by one of the ejected tube assembliesThe entire reformer section was condemned necessitating replacement
Pre Incident General Radiant Tube External Arrangement Post Incident External Damage
Tube 161 lifted approximately16 ft (view looking up)
Internal condition of radiant section
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FAILURE MECHANISMPrior to start-up water was present in the feed system upstream of the radiant tube sectionAs the Process Steam flow was ramped up per the startup procedure (increased mass and velocity) it picked up water and carried it into the radiant tubes Water introduced into tubes underwent an rapid phase change generating an extreme local pressure impulse and shock wave. The wave initiated longitudinal cracking
– Entrained water impinged on hot (350oC) catalyst and possibly the pipe wall,”instantly flashing”
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A B C
D E F
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ROOT CAUSEAccumulated water was not removed upstream of the radiant section prior to introducing steamThe Mixed Feed Preheat Coil is the most probable location where water was pooled prior to the event because:
– Steam could have collapsed into water in the system after shutting down or from passing valves
– Inlet header is not self draining – The outlet header is the low point
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LESSONS LEARNEDInadequate Safeguards:
– Insufficient size and location of drains to ensure all remnant water is removed
Inadequate Procedure:– The startup procedure did not account for a startup
of a cold furnace with no hold points– Insufficient information for operators to detect a wet
system
Lack of MOC – The startup procedure has two hold points for
refractory dry out and new catalyst reduction, during the heat up phase prior to introducing the 600psig startup steam.
– These hold points were not utilized since the neither was required
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LESSONS LEARNED…Non-essential Personnel
– At the time of the incident seven people were on the furnace structureOnly the operations personnel were essential