K M Tandon

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    Efficiency improvement and cost optimization inFertiliser Plant- Case Study

    K M Tandon

    Session III III/

    Efficiency improvement and cost optimizationin Fertiliser Plant- Case Study

    Shriram Fertilisers & Chemicals : Kota

    Shriram Fertilisers & Chemicals Shriram Fertilisers & Chemicals Shriram Fertilisers & Chemicals Shriram Fertilisers & Chemicals Shriram Cement Works Shriram Cement Works Shriram Cement Works Shriram Cement Works

    Fenesta Building Systems Fenesta Building Systems Fenesta Building Systems Fenesta Building Systems Shriram Polytech Shriram Polytech Shriram Polytech Shriram Polytech

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    Location

    475 km fromDelhi on themainwesternbroad gaugeline linefrom Delhi toMumbai

    235 km fromJaipur onthe NH 12From Jaipurto Jabalpur

    Location

    Manufacturing FacilitiesPLANTS / PRODUCTS UNIT CURRENT

    PRODUCTION LEVELS

    Power MW 133

    Fertiliser - Ammonia- Urea

    TPDTPD

    7001200

    Chlor Alkali - Caustic Soda- Chlorine Liquefaction- HCl- SBP

    TPD

    325180175

    35

    Plastics - Calcium Carbide

    - PVC Resin

    TPD

    340

    200Cement TPD 1200

    Shriram Polytech - PVC Compounds TPD 60

    Fenesta - Window and Door profiles TPA 3000

    Common Services Rly. siding, Mech. Workshop, CentralStores, HR, Adm., IT, Accounts etc.

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    Fertiliser Plant

    Fertiliser Plant

    Commissioned in 1969 with a capacity of 450 TPD Ammonia / 700 TPD Urea

    Expanded in 1974 to 600 TPD Ammonia / 1000 TPD Urea

    Present Operation level is 700 TPD Ammonia / 1200 TPD Urea

    Ammonia Plant based on Haldor Topsoe Steam Naphtha reforming process

    Urea plant based on Stamicarbon's total recycle process with crystallisation route

    for urea finishing

    Ammonia plant modified to use Natural gas and naphtha in any proportion in 2006

    Plant started using gas from Sep.07

    Plant running fully on natural gas since May,2009

    Focused on reducing energy consumption

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    Philosophy of improving energy efficiency

    Identification of process bottlenecksIncreasing capacity utilisation

    Incorporation of available retrofits

    Systematic equipment replacement plan

    Reduction in shutdown frequency and duration

    Relook into original design of equipmentModifications in compression equipment

    Redesign of boilers and exchangersSimplification of piping and replacement to decrease PChange of packings

    Philosophy of cost reductionSteam conservation

    Reuse and recycle of water

    Cooling water treatment

    Water conservation

    Use of right temperature

    Trap management

    Online leak sealing

    Better procurement strategies for cooling water chemicalsBenfield system chemicals

    Reoxidation cooler for V2O5Better house keeping and maintenance practices.

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    Philosophy of cost reduction

    Compressor partsImport substitution

    Vendor development

    In house NDT

    Vibration monitoring

    Reclamation and reuse of old parts

    Replacements on condition monitoring results

    Reclamation of Lubricating Oil

    Recycle tank for Urea solutionUse of Aspen for process analysis and design

    Ammonia Plant

    Reforming section

    Modifications / upgradations

    Reformer catalyst tubes MOC changed from original HK 40 toManuarite in 2000. With this ID of tubes increased from 115 mmto 131.6 mm

    A water spray tower was installed in 1980 at the downstream ofthe waste heat boilers to maintain HTS inlet temperature byadding BFW

    The primary reformer induced draft fan was also replaced with ahigher capacity one so that proper excess air of 2.5% O2 couldbe maintained

    In order to reduce the heat duty of fired preheater upstream ofprimary reformer, a steam fired heater was installed

    A convection section was added in direct fired preheaters toutilise waste heat from flue gases

    Additional heat recovery from the Reformer convection zoneby addition of extra rows of tubes in air and steam coils

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    Carbon dioxide removal and beyond

    25 mm Metallic (SS) Pall rings were installed in the top twobeds and 38 mm rings were installed in the bottom two beds inplace of ceramic rings

    In order to reduce gas velocities at the CO2 Absorber outlet anadditional Separator was installed in 1979 itself . This helped inavoiding liquid carryover to the methanator

    To reduce the temperature of the bottom to top potassiumcarbonate solution a larger size HPC cooler had to be installedin 1983

    The synthesis gas compressors which are motor drivenreciprocating machines posed a bottleneck in achieving fullplant loads. The cylinder bores of 1st stage were increasedfrom 289 to 305 mm as there was some margin in the motor.This enabled a capacity increase of 9 %

    Modifications / upgradations

    Period between turnarounds

    Earlier the plant turnarounds were taken on annual basis.However, the IBR later allowed operation of waste heat boilersupto two years.

    With judicious planning of the overhauling of the reciprocatingcompressors the turnaround are now taken up once in two years.

    This has improved availability of plant

    Modifications / upgradations

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    Installation of a radial ammonia convertorThe original TVA Type Axial Flow Ammonia Converter Basket wasdue for replacement in 1992

    A radial flow converter was installed as replacement of old axialflow basket

    This has made the running of smaller 120 TPD AmmoniaSynthesis loop unnecessary

    Since the loop did not have any waste heat boiler, the energy wasbeing wasted to the cooling tower. This could be avoided with theinstallation of the radial converter

    Modifications / upgradations

    Feed stock conversionfrom

    Naphtha to Natural Gas

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    Why change to Natural gas

    Energy cost constitutes about 80% of total cost of production of urea

    After removal of APM from naphtha, its prices touched a very highvalue of Rs. 55,000/MT

    Gas is a clean fuel as compared to naphtha

    Gas is cheaper as compared to naphtha

    Reduced cost of production leads to improved competitiveness

    Favourable government policy for feedstock changeover

    Reduced subsidy outgo

    Conversion to Natural Gas

    Modifications done in the plantto enable it

    touse natural gas

    Conversion to Natural Gas

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    Replacement of all 252 burners from self aspirating naphtha firedburners to forced draft Natural gas / Naphtha fired burners

    Installation of a Combustion Air preheater

    This was necessary as the reformer furnace was originally designedfor 450 TPD only and it was difficult to fire sufficient heat withoutthe preheating of combustion air

    Installation of a new feed Natural Gas preheater

    Installation of new FD Fan and ID Fan at ground floor

    Installation of fuel NG preheaters

    Replacement of Steam Naphtha Coil and inlet distribution headersfor steam naphtha mixture going to the catalyst tubes

    Removal of BFW Coil from convections section of primary reformerfurtnace

    Conversion to Natural Gas

    Control system upgradation

    35 year old pneumatic controls required frequent maintenance andwere facing obsolescence

    More accurate control helps in better optimization of plant parameters

    Temperature scanner was also error prone and inaccurate

    Plant interlocks were relay based

    Old pneumatic controls replaced by state of the art Digital control System

    This has enabled

    Centralised Operation MonitoringProcess behaviour analysisMonitoring of Alarm managementProcess history storage

    Conversion to Natural Gas

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    DCS Chosen isEmersons Delta V system

    Plant safety interlocks have been implemented in integrated Delta - V SISwhich is TUV approved system for SIL3 applications.

    Salient features are

    1100 Nos I/OsEase of operationTrends , process history, alarms available.Built on commercially available personal computers as work station andengineering satations.Windows platformProven ethernet communication technologyScalable to add more controllers and operating stations as required

    Conversion to Natural Gas

    SIL safety system

    Foundation field bus

    Latest technology foundation field bus has been used for temperatureSignals and few pressure and flow monitoring requirements.

    Asset management system

    Delta V AMS suite has been installed for centralised configuration ,diagnostics, maintenance and history record for HART and FF fielddevices.

    Operator interface

    5 Operating stations with 19 LCD monitors in a control roomScreens interchangeable in all respectsOperator can scroll through the entire plant seamlessly.

    Conversion to Natural Gas

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    Redundancy

    100% plant availability ensured

    Controller 1 HDS, Gas Purification and synthesis sections

    Controller 2 Primary and Secondary reformer and LNG system

    All critical Inputs/outputs are connected to redundant modules

    Hazardous area interface

    Input cards are Delta V inherently safe . However, as a precaution

    i/o isolators for all hazardous ares have been instal led.

    Old pneumatic controls replaced by state of the art Digital control System in 200

    Conversion to Natural Gas

    Old pneumatic controls replaced by state of the art Digital control System in 2006

    Systematic effort to optimise the operation and with use of Natural Gas ,the energy consumption has been reduced significantly

    7.3257.447

    7.7147.779

    7.857.887.85

    7.81

    7.97

    8 . 0 9

    8. 28.15

    8.19

    8 . 4 3

    8 . 2 5

    8 . 3 5

    8.53

    8 . 3 8

    8.52

    9 . 0 2

    7.3

    7.5

    7.7

    7.9

    8.1

    8.3

    8.5

    8.7

    8.9

    9.1

    9.3

    9 1

    - 9 2

    9 2

    - 9 3

    9 3

    - 9 4

    9 4

    - 9 5

    9 5

    - 9 6

    9 6

    - 9 7

    9 7

    - 9 8

    9 8

    - 9 9

    9 9

    - 0 0

    0 0

    - 0 1

    0 1

    - 0 2

    0 2

    - 0 3

    0 3

    - 0 4

    0 4

    - 0 5

    0 5

    - 0 6

    0 6

    - 0 7

    0 7

    - 0 8

    0 8

    - 0 9

    0 9

    - 1 0

    1 0

    - 1 1

    MKCal/MT Urea

    Energy performance of the plant

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    Old pneumatic controls replaced by state of the art Digital control System in 2006

    Focus on reducing R & M Cost

    12.24

    13.85

    12.312

    12.33

    14.84

    5.25.8

    4.7

    7.5

    5.7

    10.7

    7.5

    10.0

    8.3

    11.0 10.5

    12.911.5

    9.7

    12.9

    13.1

    8.0

    0

    2

    4

    6

    8

    10

    12

    14

    16

    18

    20

    8 8

    - 8 9

    8 9

    - 9 0

    9 0

    - 9 1

    9 1

    - 9 2

    9 2

    - 9 3

    9 3

    - 9 4

    9 4

    - 9 5

    9 5

    - 9 6

    9 6

    - 9 7

    9 7

    - 9 8

    9 8

    - 9 9

    9 9

    - 0 0

    0 0

    - 0 1

    0 1

    - 0 2

    0 2

    - 0 3

    0 3

    - 0 4

    0 4

    - 0 5

    0 5

    - 0 6

    0 6

    - 0 7

    0 7

    - 0 8

    0 8

    - 0 9

    0 9

    - 1 0

    1 0

    - 1 1

    ( P )

    Avg. inflation rate during last 7 years 5.18% per yearGrowth rate R & M Cost during last 7 years 0.5% per year

    R & M Cost contained to below inflation rate Reduction in real terms

    Rs.Crs/Yr.

    Maintaining Plant Health with min. Capex

    1.9

    1.8

    2.813.72

    6.158.7

    8.1

    9.6

    2.2

    8.4

    4.3

    18.2

    6.0

    34.7

    6.68.0

    6.74.4

    1.8

    30.4

    1.10.92.0

    0.0

    5.0

    10.0

    15.0

    20.0

    25.0

    30.0

    35.0

    40.0

    8 8

    - 8 9

    8 9

    - 9 0

    9 0

    - 9 1

    9 1

    - 9 2

    9 2

    - 9 3

    9 3

    - 9 4

    9 4

    - 9 5

    9 5

    - 9 6

    9 6

    - 9 7

    9 7

    - 9 8

    9 8

    - 9 9

    9 9

    - 0 0

    0 0

    - 0 1

    0 1

    - 0 2

    0 2

    - 0 3

    0 3

    - 0 4

    0 4

    - 0 5

    0 5

    - 0 6

    0 6

    - 0 7

    0 7

    - 0 8

    0 8

    - 0 9

    0 9

    - 1 0

    1 0

    - 1 1

    ( P )

    R

    s . C

    r s

    .

    Average Capex Rs. 7.8 Cr./Year

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    Old pneumatic controls replaced by state of the art Digital control System in 2006

    The way forward - Energy savings schemes

    S.No.

    Scheme Expected energysavings

    MKCal/MT Urea

    A. AMMONIA PLANT

    1 Heat Exchange Reformer (KRES) 0.32

    2 Additional cell in cooling tower 0.04

    3 Chiller at synthesis gas compressor suction 0.02

    B UREA :

    1 High Efficiency Combined (HEC) process for Ureaor 1st stage heat recovery

    0.16

    2 Evaporation route for Urea Plant 0.073

    3 Additional cell in cooling tower 0.04

    4 Natural Draft prilling tower 0.02

    5 DCS and N/C Metering for urea plant 0.01

    Total (A+B) 0.683

    Thank you

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    Session III III/

    Urea concession price

    *

    11771

    8751 92809884

    12183

    18018

    23178

    19995

    8000

    10000

    12000

    14000

    16000

    18000

    20000

    22000

    24000

    SFC, Kota Pre-92 -gas

    Post-92 -gas

    Mixedfeed

    Post-92 -Naph.

    Imported FO/LSHS Pre-92 -Naph.

    Rs./MT Urea

    Comparison with other Indian plants and imported Urea