Reducing Rejection Rate in Pump Casing Assembly by Using Tpm

Post on 29-Nov-2014

123 views 3 download

description

AU Project Presentation-Sample

Transcript of Reducing Rejection Rate in Pump Casing Assembly by Using Tpm

Department of Mechanical Engineering 1

PRESENTED BY

A.Balasubramani(08030610017)

M.Devarajan(08030610026)

G.Kanagaraj(08030610049)

SUPERVISOR

Mr. R. SATHIYA MOORTHY, M.E, (Ph.D)

Assistant Professor

Dept. of Mechanical Engineering,

Anna University of Technology,

Coimbatore – 641047.

2 Department of Mechanical Engineering

Department of Mechanical Engineering 3

Objective

Reducing rejection rate in pump casing assembly

line process by using TPM.

Methodology Available To Solve Problems TPM

CFT approach

10 step approach

Quality circle

6 sigma

Department of Mechanical Engineering 4

TPM Methods to solve problem PDCA Cycle

Cause and Effect Analysis

Gap Analysis

Why-Why Analysis

Kaizen

Department of Mechanical Engineering 5

Our Method of Solving

Department of Mechanical Engineering 6

Department of Mechanical Engineering 7

Product Process Flow

Welding-1 • Projection Welding

Welding-2 • Spot Welding

Welding-3 • Projection Welding

Department of Mechanical Engineering 8

Problem Details

Product rejection rate in pump casing assembly line

is 539ppm.

Stage 1- Plan

Pump Casing Assembly Line Process is Selected For Our Project, Due to More Rejection Found (539 ppm)

Department of Mechanical Engineering 9

Department of Mechanical Engineering 10

Sl.No Process Rejection PPM

1 Projection Welding-1 92

2 Spot Welding 364

3 Projection Welding-2 83

Total 3-Process 539

Process wise Rejection Status

Department of Mechanical Engineering 11

Process Defect Rejection Qty Per 5000

Nos Rejection PPM

Projection Welding-1

Product Missed Weld 0.34 68

Dislocating 0.05 10

Improper Parameter 0.07 14

Spot Welding Misaligned Welding 1.75 350

Improper Parameter 0.07 14

Projection Welding-2

Product Missed Weld 0.305 61

Dislocating 0.05 10

Improper Parameter 0.06 12

Defect wise Rejection Details

In Spot Welding Process Misaligned Welding Rejection is more found.

Department of Mechanical Engineering 12

Department of Mechanical Engineering 13

Misaligned Welding Rejection product

Existing Method of Operating

Department of Mechanical Engineering 14

Goal is to eliminate the spot welding process rejection in pump assembly casing assembly to zero ppm within a ppm of one month

Department of Mechanical Engineering 15

Goal:-

Stage-2:- Do Analyzing the Facts :

By using Cause and effect analysis Possible causes of misaligned welding found.

By using the why-why analysis finding the solutions for the causes.

Department of Mechanical Engineering 16

Cause and Effect Analysis For Misaligned Welding

Department of Mechanical Engineering 17

Causes of Misaligned Welding

Product locating method.

Improper handling method.

Machine Operating Speed.

Training to the operators.

Human Fatigue.

Machine Parameters.

Department of Mechanical Engineering 18

Why-Why Analysis

Q1:Why Product Locating Method is Wrong?

Ans : Product Locating depends on operator

Q: Why Product Locating depends operator?

Ans : There is no proper locating fixture

Department of Mechanical Engineering 19

Solutions For Misaligned Welding

Department of Mechanical Engineering 20

Sl.No Machine Causes of Misaligned Welding Countermeasure

1 Spot Welding Product Dislocating. Providing new fixture to locating the product with proper

welding path radius

2 Spot Welding Improper handling. Providing new fixture to holding & welding the product.

3 Projection Weld Fixture material strength. Providing new fixture with proper material strength.

4 Spot Welding Machine Speed. Providing flow control valve for the incoming Compressed

air.

5 Spot Welding Operator Training. Providing enough training to the operator.

6 Spot Welding Human Fatigue. Providing new fixture to holding the product.

By Providing the proper locating Fixture the 350ppm of rejecting can be eliminated in spot welding process.

Department of Mechanical Engineering 21

Stage 3: Check

Proposed Fixture

Department of Mechanical Engineering 22

Department of Mechanical Engineering 23

Department of Mechanical Engineering 24

Process Defect Rejection Qty Per 5000

Nos Rejection PPM

Projection Welding-1

Product Missed Weld 0.2 40

Dislocating 0.05 10

Improper Parameter 0.07 14

Spot Welding Misaligned Welding 0 0

Improper Parameter 0.03 6

Projection Welding-2

Product Missed Weld 0.2 40

Dislocating 0.03 6

Improper Parameter 0.06 12

Defect wise Rejection Details After Implementation of New Fixture

Stage 4 :- Act

Monitoring the solution

Kaizen Idea Sheet

Department of Mechanical Engineering 25

Result By implementing the new welding fixture for spot

welding process rejection rate in pump assembly casing assembly is reduced to zero ppm

Department of Mechanical Engineering 26

Future Enhancement By using the electric, hydraulic, pneumatic, and

hydro-pneumatic control systems and also with the help of robots handling this operation .Also this process can be integrated with machine, so man power is not required for handling the component. The component can be moved to weld the required path by using PLC programming.

Department of Mechanical Engineering 27

References Kaizen complied by Masaaki Imai “TPM introduction,

implementation, kaizen, PDCA-Cycle”

Design of jigs, fixtures, and press tool Complied By Erik Karl Henriksen “Fixture design principles, locating principles”

Statistical quality control by Steven M.Zimmerman,Marjorie L “7 Quality tools, check sheets, pareto analysis”

Department of Mechanical Engineering 28

Department of Mechanical Engineering 29

Thank You