urship CII Award for Excellence in Energy CORE Management ... · Balco is based in Chhattisgarh...
Transcript of urship CII Award for Excellence in Energy CORE Management ... · Balco is based in Chhattisgarh...
Vision : To be a World Class Integrated Aluminium & Power Producer Generating Sustainable Value for All Stakeholders
Care
Respect
Innovation
ExcellenceIntegrity
Trust
Entrepreneurship
CORE VALUES
CII Award for Excellence in Energy Management – Metal Sector
Bharat Aluminium Company Limited
Date: 26th Aug’20
Vedanta Limited, Aluminium - BALCO | 1
WHO WE ARE
Vedanta Resources Limited is a globally diversified Natural Resources Company with interests in zinc-lead-silver, Iron ore, Steel, Copper, Aluminium, Power, Oil and Gas.Our dynamic portfolio follows a history of consistent geological discovery, technological advancement and sustainable development. With a business model focused on growth, expansion and value creation for our shareholders, positive impact on the community, we operate in and leave a legacy of pride.Geographically, our operations are centered in India, Africa and Australia with over 65,000 employees.Vedanta Values are vital part of our culture and an essential underpinning of our growth and success.We are empowered to drive excellence and innovation; we demonstrate world-class standards of governance, safety, sustainability and social responsibility. Our business was built with a simple mission envisioned by the group’s Chairman, Mr. Anil Agarwal – "To create a leading global natural resource company."
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Bharat Aluminium Company (BALCO) has made significant contributions as the1st PSU in India’s Aluminium sector Incorporated in 1965, BALCO is India’s firstintegrated Aluminium business.
One of the first disinvestments of the Government of India. It now a part ofVedanta Limited, with 51% stake held by Vedanta Limited and 49% held byGovernment.
Balco is based in Chhattisgarh State having Captive Bauxite mines in Mainpatand Kawardha, Captive coal mines in Chotia, 2010 MW power generationcapacity and 5.7 LTPA Aluminium Smelting capacity at Korba Complex.
Balco produces Wire Rods, Ingots, Alloy Rods, Alloy Ingots and Rolled Products.Balco is also selling Power to State Utilities & own sister concerns.
Balco has been India’s first to have - Captive Power Plant, to venture into +300kA Prebake pots, to produce Alloy Rods for conductors used in powertransmission industry, to roll material for Aerospace Industry, online riserreplacement, busbar insulation in Pot Room, single beam implementation andholds patent for aluminium cell fuse technology.
BALCO-A Snapshot
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Vision, Mission & Core Values
“To be a world class integrated Aluminium andPower producer generating sustainable value for allstakeholders”
• To be amongst top decile in global cost curve.• Operational Excellence.• Ensure resource security with efficient supply chain.• Effective collaboration with stakeholders.• Unleash employee potential.• Build and strengthen brand equity.
Our Vision
Our Core Values
OurMission
Respect
Care
Innovation
Excellence
Integrity
Trust
Entrepreneurship
100
345
570
1100
0
200
400
600
800
1000
1200
FY-01 FY-05 FY-18 FY-23
Metal Production (KTPA)
270540
20102400
0
1000
2000
3000
FY-01 FY-05 FY-18 FY-23
Power Business (MW)
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Pot line Process Flow
96%
4%
FY'19-20
Thermal Energy Mkcal
Electrical Energy Mkwh
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CAST HOUSE#1
CAST HOUSE#2
CAST HOUSE#3
RP
WRM - 60,000 MTICM - 90,000 MT
SOW INGOT – 50,000 MTICM – 200,000 MT
WRM– 200,000 MT ICM – 175,000 MT
RP – 74,500 MT
Wire RodType : EC / AlloyCoil Weight : 1-2.5 Tons;Alloy Rod , Flip Coils
Ingots: EC Grade, CG Grade; Alloy Ingots. AlSiT Ingots; Saw IngotsSize : 740 mm x 170 mm x 114 mm
Rolled Products:Hot Rolled Coils & PlatesAlloy : 1xxx, 2xxx, 3xxx, 4xxx, 5xxx,
6xxx, 8xxxCold Rolled Coils, Strips & SheetsAlloy : 1xxx, 2xxx, 3xxx, 4xxx, 5xxx, 6xxx, 8xxxSlabsSize : 410 mm x 1270 mm,
410 mm x 1540mm, 410 mm x 1620 mm
BusbarsWidth: 500-1620 mm, Length: 2000-5000 mm, Thickness : 220-410 mm
BALCO - Finishing Capacity
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Balco Transformation
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30
95
160170
0
20
40
60
80
100
120
140
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FY 04 FY09 FY14 FY19 FY20
Productivity (MT/Man)
0.960.96
2.45
3.22
5.7 5.7 5.7
1.43
0.96 1.03
2.51
3.28
5.72 5.63 5.69
1.38
1794017605
14487
14438
13904
13950
13857
13848
0
2000
4000
6000
8000
10000
12000
14000
16000
18000
20000
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FY01 FY04 FY09 FY14 FY19 FY20 FY21 BP FY21 Q1
Metal Production & Power Consumption Optimization
Hot Metal Production Capacity (LTPA) Hot Metal Production ( LTPA)Sp. Power Consumption(kWh/MT)
Energy Objectives
Reduce Net Power consumption – 12865 kWh/MT of Al
Reduce Auxiliary Power Consumption of potline-1 -387 kWh/MT
Reduce Auxiliary Power Consumption of Potline-2 - 447 kWh/MT
:
Reduce Net AC Power consumption for
Potline-1 (13302 KWH/MT to 13156 KWH/MT) - 146 kWh MTPotline-2 (13610 KWH/MT to 13425 KWH/MT) -185 kWh/MT
Reduce Auxiliary Power Consumption of potline-1 from 461 to 447 KWH/MT-13 kWh/MT
Reduce Auxiliary Power Consumption of Potline-2 from 493to 469 KWH/MT - 24kWh/MT
ENERGY OBJECTIVES (FY 21) : ENERGY OBJECTIVES (Vision FY23)
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International Benchmark National Benchmark BALCO Vision
Pot-line DC Specific-Power kWh/MT &Benchmarking
1348013430
13295
13380 13380
1285612800
12900
Qat
alu
m
Du
bal
Mad
en
Alb
a
Emal
Alo
uet
te
Pin
ggu
o
We
iqia
o
13512 13485
13100
13523
13356
12982
13386
13197
Hin
dal
co M
ahan
Ad
itya
Alu
m
VA
L P
lan
t 1
VA
L SE
Z
VA
L (W
A)
Bal
co P
L 1
Bal
co P
L 2
Bal
co
12918
12725
FY 2
02
1-22
FY 2
02
2-23
** Balco is benchmark in Indian & Gulf smelters in DC Specific Power Consumption
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Energy Conservation Vision 2023
5956.9 55.9 55
52.94 52.1 52.8 51.649.3
FY-13 FY-14 FY-15 FY-16 FY-17 FY-18 FY-19 FY-20 FY-23
Specific Energy Conservation Journey (GJ/MT)
VISION 2023
S. No. Major Projects / Action Plan for Vision FY23 Power Saving UnitTarget
Completion
1 Increase in Pot-line Current Efficiency from 93.9 to 94.63 109 Kwh/MT Mar-21
2 Reduction in Pot-line Aux. power consumption 19 Kwh/MT Mar-21
3 Installation of 100% graphitized Cathodes 228 Kwh/MT Mar-22
4 Up gradation of Pot-control system in Pot-line 2 417 Kwh/MT Mar-22
5 Replacement of conventional motors with energy efficient motors 230 Kwh/MT Mar-22
6 Cast iron sealing in cathode 30 Kwh/MT Mar-23
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52.153.9
52.1 53.02
FY 18-19 H-1 H-2 FY 19-20
Axis Title
Specific Power Consumption (GJ/MT)
Reason for Variation in Energy Consumption FY20
** Due to flood in plant on Aug’19, water entered in Rectifier (RCW) & potlinebasement resulting in stoppage of 36 pots . Thereby increasing the DC power consumption in potline.
Glimpses of Flood
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Major Energy Conservation Projects-2017
S.No Title of ProjectAnnual Energy
Saving Million KWH
InvestmentMillion
INR
1 Increase in Pot-line Current Efficiency from 93.38 to 94.48% to save 140 KWH/MT 46.26 NIL
2 Cathode upgrade & Process optimization in Potline-1 & 2 to save 500 KWH/ MT 9.58 12
3 Modification in Cooling tower wheel with FRP in Cast House-3 0.06 0.81
4 Installation of VFD for Hot well pumps Cast House 3 0.47 1.55
5 ID fan motor overhauling and bearing replacement for FTP1 0.22 0.12
6 Pre-Heating f/c power saving by reducing temperature of heaters during PM/SD 0.14 NIL
7 Load shifting from under loaded transformers 0.42 NIL
8
Optimization of running hours of FTA vacuum unit(20% reduction in consumption).Safety filter of FTA1 & 2 changed to increase suction rate of sucking pipe
0.15 0.03
9Closed looping in cooling pump house of Air compressor house-1(Potline-1) & Rectifier Pump House -2(Potline-2)
0.5 4.5
TOTAL (ROI-4 Months) 57.8 19.01
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Major Energy Conservation Projects-2018
S.No Title of ProjectAnnual Energy Saving
Million KWH
InvestmentMillion
INR
1 Increase in Potline1 Current Efficiency from 94.11% to 94.39% to save 42 KWH/MT 8.32 NIL
2 Cathode upgrade & Process optimization in Potline-1 in FY 19 (89KWH/MT). 26.53 616
3 Pot controller modification in Potline-1 to save 219 KWH/ MT(GAMI) 66.25 200
4 Auxiliary Energy Consumption reduction in to save 16 KWH/ MT 9.87 NIL
5 Cathode upgrade & Process optimization in Potline-2 in FY 19.(107KWH/MT).25.56 682
6 Auxiliary Energy Consumption (inc TL) reduction in to save 15 KWH/ MT 14.76 NIL
7 Replacement of conventional MH400 W roof light fittings with LED 200 W (50 no's) 0.032 0.5
8 Roof light replacement 120 no's with LED. (10 no's per month)0.068 1.2
9 Replacement of 250 W HPSV to 90 W LED in Street Lights0.48 1.5
10 Modification in Cooling tower blade with FRP 0.18 1.5
TOTAL (ROI- 18 Months)152.05 1502
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Major Energy Conservation Projects-2019
S.No Title of ProjectAnnual Energy
Saving Million KWH
InvestmentMillion
INR
1 Increase in Potline1 Current Efficiency from 94.28% to 94.65% to save 56KWH/MT11.02 NIL
2 Cathode upgrade & Process optimization in Potline-1 40 pots in FY 20(55KWH/MT). 12.53 304
3 Increase in Pot line 2 Current Efficiency from 93.85% to 94.38% to save 79 KWH/MT 10.98 NIL
4 Cathode upgrade & Process optimization in Potline-2 102 pots in FY 20.(142KWH/MT).15.55 561
5 Bake oven-Duct leakage arresting in FTP duct leading to a a reduction in ID fan speed by 2 %.0.12 NIL
6Ach Potline-2 Reduce the operating pressure of pumps in line 2 compressor pump house by VFD installation)
0.08 1.6
7 GAP- HTM heater oil change0.08 NIL
8Foundry -Optimising Temperature set point of all holding furnace 0.01 0.03
TOTAL (ROI- 18 Months) 50.37 866
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Installed 33 KW Grid connected Solar power plant.
Biomass Pilot Trial taken successfully at BALCO CPP#2(4X135 MW) in month of June-20,Total 125 tons of biomass was blended from 3%to 10 %to check technical feasibility as per MNRE guideline line
230 acres land has been identified within BALCO and feasibility Study done internally. Vendor exploration Initiated. 1.5 MW roof topSolar.
Utilization of Renewable Energy
Biomass Pilot triaktaken successfully
Long term plan of biomass cofiring
under progress to reduce green house
gas emission
Land Identification for Solar Plant & Feasibility Study
planning initiated
Solar Plant Vendor identification & roof top solar Proposal
Plan initiated
Exploration of Long term PPA with Hydro
plant
Identified Land in BALCO for Proposed Solar Plant Installation
Chotia mines Ash Dyke Township BCPP CHP Yard Brown Field Land
Roof Top Solar Installation
within BALCO
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Innovation-Project 1
Project Title:
Utilization of LP compressed air for FTP Line-2 operation to reduce Auxiliary power consumption.
Project Details:
Modification done in HP(high pressure) pipeline and LP(low pressure) pipeline to run FTP operation by LP compressed air instead of HP compressed air which results into reduction in power consumption by 12 MWH/day.
Study of Pressure and flow (by internally and third party also) to run FTP operation by LP compressed air and its impact on FTP operation as well as power consumption.
Pressure setting of pressure regulating valves(PRVs) changed. Before 6 bar pressure from HP Line used for operation after modification it is changed to 4 bar.
Compressor house
Pipeline NetworkHP#5
HP#4
HP#1
HP#2
HP#3
LP#1
LP#2
Pot Room+Cast
FTP+BakeOven
Rodding+LCS
Al Handling
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Analysis
From detail analysis of compressor design capacities, efficiency, study of pipeline network, FTP pressure and flow requirement. It was found that we can run FTP operation by LP compressed air in which we will supply 4 bar compressed air instead of 6 bar from HP line.
Analysis of Power consumption of compressor house.
Pipeline network Compressor efficiencies Area wise Flow study
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Implementation
Action Plan
In-house modification with our own resources. MOC Making and approval for implementation in shop floor Fabrication of U bend to interconnect LP and HP pipeline. Arrangement of 350 mm butterfly valve Shutdown of FTP and alumina handling to interconnect pipeline Fitting of 350 mm valve in both the pipeline HP and LP line separately. Requirement of pressure for FTP operation is approx. 2.5 bar so change setting
of pressure regulating valves as per operation by LP compressed air.(from 6 bar to 4 bar)
Data calculation for Power consumption of compressor house. By these calculation and implementation we found that we can save approx.
12 MWH/day by utilizing low power consuming compressor for FTP operation instead of high power consuming compressor as used previously.
HP#5
HP#4
HP#1
HP#2
HP#3
LP#1
LP#2
Pot Room+Cast
FTP+BakeOven
Rodding+LCS
Al Handling
Before modification
After modification
HP#5
HP#4
HP#1
HP#2
HP#3
LP#1
LP#2
Pot Room+CastHouse
Rodding+LCS
Al Handling
FTP
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Results Achieved & Benefits
Power Saving calculation
1 day power consumption by HP compressor:39 MWH /day 1 day Power consumption by LP compressor :27 MWH/daySimilarly from energy report Daily Compressor house Power consumption before: 167 MWH After Daily Compressor house Power consumption :155 MWH Total per day power consumption saved :12 MWH Cost Saving per Day :12*3*1000:36000 INR Hence Annual Saving :36000*365: 13,140,000 INR Excess of LP compressed air utilized. Decrease in compressor vibration fluctuation. LP compressor tripping reduction due to surge Risk Reduction of alumina Bulker bursting
Parameter
Before After
(Avg./month)(Avg./m
onth)
Potline 2 Power
Consumption
(MWH/Day)
167.25 155
Vedanta Limited, Aluminium - BALCO | 20
Graphitized Cathode with copper insert collector bar design
The Aluminum production is an energy intensive process. To be more costefficient, the process needs to be more energy efficient. Energy efficiencydepends mainly on the technology used and relining materials being used.In a electrolytic cell, energy consumption can be reduced by reduction ofvoltage drop & Increasing the pot life.
To collect the historical data, pots were chosen having same cell design,located within same pot line and similar age. Cathode voltage drop (CVD)and wear rate of cathode were taken as performance indicator.
Project Title :
Project Details
Data Collection
Innovation-Project 2
Pot Cell – Side View
Pot Cell – Front View
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1. In electrolysis process, generates horizontal & vertical component of electric current between anode & cathode. High Horizontalcomponent indicates high noise, Voltage swing. High vertical component indicates pot stability means high CE & high life. This verticalcomponent can be increased and horizontal component can be reduced by inserting the copper plate in Collector bar .Through this,collector bar resistivity will also reduce (improving the cell magneto-hydrodynamic (MHD) state).
2. Copper is high thermal conductive material so that heat dissipation will be more in copper insert collector bar so that new lining designkeeps the heat in the pot, i.e. reduces thermal losses.
Uniqueness of the project
Magnetic Field Diagram Thermal Image
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Data Analysis, Countermeasures & validation
Accuracy and repeatability of measurements is important as data is input for calculations. The higher thermal conductivity of Copper insert collector bar cathode compared to normal collector bar cathode blocks required added insulation within the cell lining to maintain the same thermal balance without increasing the energy required to operate the pot.
This operating window is defined by the thermal limits (bath freezing and melting of the ledge) and the stability of the pot. Further constraints about minimum metal output or maximum specific energy consumption can be included to understand the regions where the operation of the pot is possible,
Side Protection ledge profile for graphitized cathode + copper insert collector bar with new relining design
Side Protection ledge profile for graphitized cathode with normal collector bar
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Cathode Voltage Drop and wear rate has been substantially lowered than reference graphitized cells and leading to reduction in Specific Energy Consumption and satisfying project target.
Fig.- Comparison of measured CVD and DC power between
Reference graphitized cathodes and copper insert collector bar with
graphitized cathodes.
Results Achieved/Results Achieved
Annual benefits of 2 trial pots (in Rupees) : 6.9 lac/year /pot ( Type 1& 2: 12952 & Copper Inserted : 12650 kWh/MT , Saving- 302 kWh/MT , Metal Production- 920 MT/pot/year , Power rate : 2.5Rs/kWh)
Result
Benefits
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Previously the EMS (Electromagnetic Stirrer) was working on an Offline and stand-alone mode and there was no provision for capturing the Running hours and also no automated control over ON/OFF and totally dependent on Operator’s feedback which led to excess power consumption.(Minimum 1000 kWh/day)
Project Title:
Power Saving through Automation of EMS
Project Details:
Innovation-Project 3
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Electromagnetic Stirrer is being used in order to improve the temperature distribution inside the furnace and chemical homogenization of alloying elements like Silicon, Titanium , Magnesium, Strontium for better quality of Primary Foundry Alloy (PFA) material for our prime customers
BEFORE - The running hours of EMS unit was noted manually and also it was running 24x7 as there was no automated control system over Start/Stop of the EMS and this in-turn led to excess Power Consumption.
AFTER - In order to overcome the above shortcomings we have integrated the Furnace and EMS unit and captured the Start and End bit of the EMS and calculated the time . We have installed a large LED at shop floor, a provision to display the Current status of EMS to the operator through Green and Red indicators . We have shown the critical parameters of BEFESA , Furnace, EMS so that anyone in shop floor can get a clear view of current status. Also programming in PLC has been made in such a way whenever furnace is in tilt position EMS stops immediately without any manual intervention through reed switch relay.
EMS Running Condition EMS Running Time
Analysis & Action
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Project Effect
All the Stand-alone units like EMS, Furnace and Alloy ICM have now been integrated via common network platform in Historian server through critical tag values and using MES this automation has been achieved. Also programming has been made in such a way whenever furnace is in tilt position EMS stops immediately without any manual intervention through reed switch relay. One LED has been provided at Shop floor for the same.
Limit Switch Interlock for EMS in Programming
Limit Switch
Programming Implementation
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Power saving of 300 MWH/Year which will give net saving of 0.23 $/MT/Year and fulfilled the Customer requirements of Hero MotoCorp ,Enkei, Kosei Minda for best practices in shop floor
Through Implementation of Automation of EMS following Cost benefits will be achieved:
As per OEM in Full capacity 6 Cast per day is proposed, Power requirement before project was 6*950=5,700 kWh . After completion of the project the Power consumption is expected to reduced by 6*780=4,700 kWh
Power saving= 1,000 kWh/dayApprox.it saves 25,000 kWh per month
Cost of Power=2.3 Rs./Watt
Therefore Total Cost Saving = 2.3*25*1000= Rs.57,500 per Month
Total Annual Savings = 57,500*12= 6.9 Lacs/Year
Net Savings = 0.23 $/T/Year
Results Achieved/Results
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Plant 1 water allocation reduction from 0.69 MCM to 0.64 MCM (savings 3.6 Cr in a year).
Designated Consumer under PAT scheme for Aluminum Sector. PAT cycle -1 target over achieved by 0.088 TOE (awarded 22203 EScerts).
PAT cycle-2 Target: 5.0275 TOE/MT by 2018-19,Till date performance - 3.31TOE/MT
Environment Management Initiatives
3.4 Zero Waste
ZeroDischarge
Zero Harm
HSE VISION
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Specific Water Consumption (KL/MT)
0.79
0.720.69
0.64
0.44
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Waste to Wealth
Medium Term
LongTerm
ShortTerm
SPL
Annual Generation
5130 MT
Co-Processing with SPL detoxification plant
Set up of SPL Detoxification plants(Under CPCB Approval)
Explore for Blast furnace injection as fuel, As Flux for Steel making or as reducing agent for slag cleaning
Al Dross
Annual Generation
8000 MT
Maximising Al recovery by increasing utilisation of DPM to 95%
1350 MT Metal recovery from DPM
Melt loss Reduction -0.5%
Using Dross as raw material in refractory manufacturing
13.8 Cr FY20 YTDMS Scrap
5.3 Cr FY20 YTDCoke Dust
4.8 Cr FY20 YTD
9.1 Cr FY20 YTD
Dross
Others
3224 MT/year Co-processing at M/s Green-mech Technology
1906 MT kept at SLF
Drosses and waste from treatment of salt sludge - 6507 MT
Used Oil sellout – 78.45 MT
Empty barrels /containers/liners contaminated with Haz ChemWaste – 2498 Nos
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GHG Inventorisation
YearScope 1 emissions KG CO2/Ton of Final
product
Scope 2 emissions KG CO2/Ton of Final product
Total KG CO2/Ton Final product
2014 - 15 23.3 2.3 25.6
2015 - 16 18.24 0.2 18.44
2016 - 17 18.85 0.03 18.88
2017 - 18 17.28 0.27 17.55
2018 - 19 17.35 0.05 17.41
2019 - 20 17.78 0 17.78
Plantation Drive
FY 15 – 183700FY 16 – 102500FY 17 – 87000FY 18 – 92500FY19 – 30000FY20 - 15000
Plantation Drive
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Green Supply Chain & Ongoing Plans with Various Vendors
SN Initiatives Savings
1 BTAP Capacity Enhancement 396 GJ/Month
2 Use of Higher Capacity Truck( from 16MT to 25MT) 1697 GJ/Month
3 Use of 12MT instead of 6MT ladles & Energy efficient
engine
116 GJ/Month
4 Use of GPS to identify shortest route
200 GJ/Month
5 Door to Door delivery initiative for issue of material
from stores
6 Transportation of finished goods in Container rake
7 Use of Re-Fuelling Vehicle
Sl.
No.
Name of the
Vendor
Description of the Collaboration / energy
reduction initiative
1 SGL For energy efficient cathodes
2 GAMI & AP Pot controller upgradation
3 SKF For energy efficient bearing & V-belts
4 EESL Energy Efficient Motor replacement
5 Atlas Copco Compressed Air Audit
Implementation of Best PracticesIdea Portal & !DEA@BALCO APP for generation of ideas for All Balco & Contract employees. Idea generated FY20 – 9741 Idea accepted FY20 – 4606 Idea implemented FY20 – 3446 Idea under implementation FY20 – 1160
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Energy savings from Employee & Stakeholder Involvement
23%
34%
56%48%
72%
0%
10%
20%
30%
40%
50%
60%
70%
80%
FY 16 FY 17 FY 18 FY 19 FY 20
Involvement at Balco
Details Unit 2015-16 2016-17 2017-18 2018-19 2019-20
QCs & Kaizen Projects Implemented
No. 121 1277 2019 2629 6544
Energy Savings Kwh 4375000 26892304 59584971 25367013 31381627
Benefits due to energy savings
Rs. lacs 131 806 1788 887 1098
35 Gold & 3 Silver Awards in Chapter Conventions, 8 Par excellence & 7 Excellence awards at National convention (QCFI).
121
12772019
2629
6544
3.2
42
24
35 32
0
5
10
15
20
25
30
35
40
45
0
1000
2000
3000
4000
5000
6000
7000
FY16 FY17 FY18 FY19 FY20
Projects & Benefits Trend
No. of Projects Benefits in Crores
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Creating Awareness Among Stakeholders
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# Description Certification Benefits
1 Quality management system ISO 9001:2015 Enhanced customer satisfaction and improved customer loyalty leading to repeat business , Increased revenue and market share obtained through flexible and fast responses to market opportunities, Consistency in the delivery of your product or service.
2 Environment Management System
ISO 14001:2015 Identify cost savings with greater emphasis on resource, waste and energy management, Demonstrate compliance with current and future statutory and regulatory requirements.
3 Occupational Health & Safety Management System
OHSAS 18001:2007 Give signals to our clients and stakeholders that our organization is committed to protecting the needs of all our stakeholders.
4 Energy Management System ISO 50001:2011 Increase energy cost savings for the organization by reducing costs via a structured approach to managing our energy consumption.
5 Asset Management System ISO 55001:2014 Better management of risks, Enhanced brand reputation , Improved financial performance.
6 Quality Management System for the automotive industry.
IATF 16949 Ability/helps to enter auto manufacturing market.
7 Information Security Management System(ISMS)
ISO/IEC 27000:2013
Safeguard our valuable data and intellectual property
8 NABL accredited Lab ISO 17025:2005 Reliable testing, measurement and calibration services
9 Social Accountability SA8000 Addresses and prevent social and labor risks, motivates worker engagement
Energy Policy & Certifications
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Status of EnMS (ISO 50001) Audit Observation
Year No. of NC No. of Observation Open NC Open Observation
Balco 15-16 3 17 0 0
Balco 16-17 0 10 0 0
Balco 17-18 0 6 0 0
Balco 18-19 0 5 0 0
Balco 19-20 0 3 0 0
%Investment for Major Energy conservation projects on Turnover
FY Project DescriptionInvestment
(Rs. Crs)Turnover (Rs.
Crs) % Investment on
TurnoverROI
(Months)
2017-18Pot Controller up gradation Pl-1 and 100% GraphitizedCathodes
132 9063 1.4% 18
2018-19Projected investment –Pot controller up gradation Pl-2 & Energy efficient cathode
183 9063 2.0% 20
2019-20 100% Graphitized Cathodes 138 10500 1.3% 18
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Best Paper Presentation Award on” Development& Stabilization of A356.2 Alloy Ingot “-IBAAS
Golden Peacock Award inEnergy Efficiency Category
CII HR Excellence AwardAON Best EmployerAward
Sustainable Business of the Year Award
IMEA Future ReadyFactory Award (PlatinumCategory)
RBNQA PerformanceExcellence Trophy
The ET 4 Good Award
Sustainability 4.0 Award
Energy & Environment Global Environment Award
Future of Procurement Award PR Best Practices Award D L Shah Award
Golden Peacock Award inCSR
Awards
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Corporate Social Responsibility
Strengthened 330 SHG’s.
1087 linked to IGA.
Mushroom Produced: 20,710 Kgs
Earnings: Rs 3,581,800
Spawn Production: 21,442 Bottles
Earnings: Rs 480,000
Established Bio-flock for fisheries.
790 acres brought under secured irrigation.
SRI Cultivation in 235 acres
Wheat Cultivation in 110 acres
No. of farmers benefitted: 600
Total Earning: 1.89 Cr
Providing training to youths in 6 trades.
736 trained and placed.
45-60 days training program.
Earning 9500-10,000 per month
Door to Door awareness: 4000 HH
SHG Awareness program: 1012 women.
28 Adolescent girls group formed.
Currently running 5 Rural Health Post
Catering to the needs of more than 60
villages.
17664 people benefitted through RHP
3429 people covered through HIV
awareness.
2756 benefitted through programs on
women & child.
Vedanta Limited, Aluminium - BALCO | 38
Awareness & Relief activities against Covid -19
Awareness activities about Do’s & Don’ts in both Rural & Urban
areas with the help of mic & Pamphlets
Pamphlet for awareness generation
More than 15 K masks produced by SHG members,
earning 75 K.
Continuous Sanitization drive in 22 Villages and 11 Urban
communities.
More than 12000 cooked meals distributed to families dependent on daily wages.
Vedanta Limited, Aluminium - BALCO | 39
Sanitation kits including soaps & Masks distributed to 3250
HHs in 6 Panchayat
Created 100 bed isolation hospital in association with
District Administration
1000 PPE kits given to AIIMS Raipur
• Providing Farm fresh vegetables.
• Direct link between Farmers and end customers.
• Managed by KKUPCL, a farmer producer company promoted by BALCO.
• 135 customers.
1190 Dry Ration Packets distributed to families under
BPL and daily wage.
Protection & Cure activities against Covid -19
Vedanta Limited, Aluminium - BALCO | 40
THANK YOU