Study of the Effect of Blast Pattern Design on Autogenous ... Adjusting blasting to increase SAG...

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Study of the Effect of Blast Pattern Design on Autogenous and Semi-Autogenous Mill Throughput at Gol-e-Gohar Iron Ore Mine Authors: A.Hakami, H.Mansouri, M.A.Ebrahimi Farsangi, M.R.Dehghan and F.Faramarzi Presenter: Farhad Faramarzi

Transcript of Study of the Effect of Blast Pattern Design on Autogenous ... Adjusting blasting to increase SAG...

Study of the Effect of Blast Pattern Design on

Autogenous and Semi-Autogenous Mill Throughput at Gol-e-Gohar Iron Ore Mine

Authors: A.Hakami, H.Mansouri, M.A.Ebrahimi Farsangi, M.R.Dehghan and

F.Faramarzi

Presenter: Farhad Faramarzi

• Previous works

• About Gole-e-Gohar iron ore mine (Mine No.1)

• Fragmentation measurement

• SAG power index (SPI) test

• Conventional blast pattern vs. new blast pattern

• Mills performance before and after implementation

• Conclusions

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Table of contents

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Previous works

• The Mine to Mill concept (McKee, 1990)

• The relationship between fragmentation in mining and comminution circuit

throughput (McKee, 1995)

• Exploring the effect of blast design on throughput at KCGM (Kanchibotla et al., 1998)

• Blasting for reduced process plant costs at Argyle diamond mine (Bulow et al., 1998)

• Mine to mill blasting to maximize the profitability of mineral industry operations (Kanchibotla., 2003)

• Blast fragmentation for maximising the SAG mill throughput at Porgera gold mine (Grundstrom et al., 2001)

• Effect of Blasting on the Strength of Rock Fragments (Kemeny., 2003)

• Optimum blasting? Is it minimum cost per broken rock or maximum value per

broken rock? (Kanchibotla., 2003)

• Optimisation of the Cadia Hill SAG mill circuit (Hart et al., 2001)

• Adjusting blasting to increase SAG mill throughput at the Red Dog mine (Paley et al.,

2001)

• Mine to mill optimisation for conventional grinding circuits – a scoping study (Jankovic and Valery ., 2002)

• Process integration and optimisation; a case study in productivity improvement (Dance et al., 2007)

• The influence of blasting on Kemess hypogene ore milling (Hikita, 2008)

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Previous works

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Throughput gains of 5-15% have been recorded and confirmed at operations

with SAG mills such as (Jankovic and Valery ., 2002):

• Highland Valley Copper (Canada)

• Minera Alumbrera (Argentina)

• Cadia (Newcrest Mining in Australia)

• Escondida (Chile)

• Porgera (Placer Dome in Papua New Guinea)

• OK Tedi (BHP in Papua New Guinea)

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Previous works

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About Gole-e-Gohar iron ore mine (Mine No.1)

Gyratory Crusher

Crusher Stock piles

Bins

Line 3- AG 9m×2.05m

Line 1- SAG 9m×2.05m

Line 2- AG 9m×2.05m

Line 4- HPGR

Thickener Concentrate Stock piles

Crusher closed side set was 20 cm SAG : Operated at 5% ball charge Critical speed for SAG/AGs: 85% Mills are operated in dry mode Mills are air swept

Muck pile and Mills’ feed size distribution:

• Split-Desktop was used to carry out image analysis.

• Delineation was done manually and the 100% fines correction option used.

• Photos were taken by a digital camera during the excavation of muck piles.

• Stock pile distribution was also photographed before, during and at the

end of implementation.

• It was not possible to stop the belts for sampling and sieving belt cuts.

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Fragmentation measurement

• MinnoveEX SPI test developed by Starkey and Dobby, 1996. • It’s a laboratory batch test to evaluate comminution behavior

rocks and also SAG mills specific energy (Amelunxen et al., 2014).

• Why SPI? It was the only available equipment for evaluation ore hardness at Gol-e-Gohar laboratory.

• How SPI was done? The time required to; 2kg sample (F80<12.7mm) 2kg sample (P80<1.7mm)

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SAG power index (SPI) test

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Conventional blast pattern vs. new blast pattern

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Mills performance before and after implementation

Throughput: 30% Energy : -21% Throughput: 5%

Energy : -4% Throughput: 14%

Energy : -14%

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Mills performance before and after implementation

374

524 472 485

549 538

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1 2 3

Trou

ghpu

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Mill Number

Old blast pattern New blast patternNew Blasts

April May June July August September October November December January February March

• For the first time in Iran, a mine to mill blasting approach

implemented at Gole-e-Gohar iron ore mine No.1, “ A Good Start”.

• By increasing powder factor from 1.65 to 2.48 kg/m3 by a tighter

blast pattern and so finer ROM distribution; up to 30% increase in

throughput and also up to 21% decrease in the mills’ energy

consumption achieved, “A Good Result”.

• Studies should continue at Gol-e-Gohar iron mine by more blast

practices and comminution tests; if key decision makers accept the

concept/changes “A Sweet Hope” .

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Conclusions

Shahid Bahonar University of Kerman

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Acknowledgements

Gole-e-Gohar Mining and Industrial Company

Gol-e-Gohar Iron and Steel Research Institute

Thank You! Questions?