REDUCTION OF CYCLE TIME IN SCREW AIR COMPRESSOR ASSEMBLY LINE USING KAIZEN...
Transcript of REDUCTION OF CYCLE TIME IN SCREW AIR COMPRESSOR ASSEMBLY LINE USING KAIZEN...
International Journal of Lean Thinking Volume 6, Issue 2 (December 2015)
REDUCTION OF CYCLE TIME IN SCREW AIR COMPRESSOR ASSEMBLY LINE USING KAIZEN SURVEY
D. Rajenthirakumar*
PSG College of Technology, Peelamedu, Coimbatore – 641004, Tamil Nadu, India E-mail: [email protected]
S. Nandhakumar PSG College of Technology, Peelamedu, Coimbatore –
641004, Tamil Nadu, India
A R T I C L E I N F O
A B S T R A C T K E Y W O R D S
________________________________
* Corresponding Author
Kaizen, Lean assembly line, Standardization, cycle time reduction.
Received 21 June 2015 Accepted 22 July 2015 Available online 1 December 2015
In this competitive world, any company has to fulfill its
customer needs to survive in the market. Lean
manufacturing is a technique that can be adopted in a
company to improve the quality of its products, reduce
the cost of the production and also deliver the
products in less time. The goal of this work is to show
the applicability of lean manufacturing’s body of
knowledge in a screw air compressor manufacturing
company. Here, the main objective is to evolve and
test several methodologies to eliminate wastes in the
assembly line as the company at present unable to
meet the customer demand.
A systematic approach is suggested for the
implementation of lean principles to showcase that
lean could be applied to the compressor assembly
line to enhance the productivity thereby making the
line more efficient. In the current assembly line there
was no work standardization followed by absence of
kaizen that has led to an increased assembly time.
Thus with the help of lean tools and techniques such
as 5S, kaizen, standardization, visual management,
poke yoke and string diagram the total cycle time has
been reduced from 236 to 209 minutes. This
reduction has benefitted the company in meeting the
customer demand, increased profit and work
satisfaction.
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1. Introduction
Lean manufacturing philosophy was pioneered by a Japanese automotive company, Toyota
during 1950 ’s. Due to its global superiority in cost, quality, flexibility and quick respond, it
was transferred across countries and industries. The influence of lean practices contributed
substantially with the operating performance of the plants and use of lean tools allows the
improvements of results. The main principle of lean manufacturing is to reduce waste in an
operation, such as long lead times, defects and material waste. In order to visually display
whether the manufacturing field is escalating and spreading more widely across the globe, it
is important for companies to adapt to the increasing and evolving business strategies.
In order to be lean the company should follow the lean principles such as (i) Specify the
value desired by the customer (ii) Identify the value stream for each product providing that
value and challenge all of the wasted steps (generally nine out of ten) currently necessary to
provide it (iii) Make the product flow continuously through the remaining value-added steps
(iv) Introduce pull between all steps where continuous flow is possible (v) Manage toward
perfection so that the number of steps and the amount of time and information needed to
serve the customer continually falls. Thus, lean implementation is focused on getting the right
things to the right place at the right time in the right quantity to achieve perfect work flow and
being flexible to change.
2. Brief Review of Literature
Chandandeep Grewal Ludhiana [1] made an attempt to initialize the implementation of lean
manufacturing system using Value Stream Mapping. A case study conducted at a bicycle
manufacturing company illustrated a lot of improvements areas with the help of current state
map. Current state map and future state map were prepared and analyzed to highlight the
benefits of a lean system in a small company. Future state was prepared after proposing some
changes in the process to reduce different wastes. QianWang et al [2] investigated a semi
automated automotive engine assembly line in which the traditional strategy of using fixed
workers in each manual assembly section is replaced by a new strategy of using walking
workers. Ajit Kumar Sahoo et al [3] research addresses the implementation of lean
philosophy in a forging company with a focus on radial forging production flow lines. The
authors used value stream mapping to identify and eliminate waste and Taguchi’s method of
design of experiments is pursued here to minimize the forging defects produced due to
imperfect operating conditions.
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Jorge L et al [4] attempted to determine the critical success factors for Kaizen philosophy
implementations. It is concluded that there is actually no Kaizen methodology that can be
applied successfully in industry, as enterprises are open systems, which react differently to a
situation and those are due to cultural aspects, social and own needs. In their paper, Martín
Tanco et al [5] showed the applicability of lean manufacturing in a seasonal food industry.
Several techniques and analyses such as value stream mapping, overall equipment efficiency,
spaghetti diagrams, work balance, and discrete event simulation were applied and analysed.
Even it was a food process industry a slight modification has been made in the existing lean
tools and been used and it presented promising improvements primarily in lead time and work
cycle efficiency.
3. Problem Environment and Objectives
The company, IJK Limited is a leading compressor manufacturer in India which produces a
range of reciprocating and screw compressor. After several brain storming and a thorough
study of the shop floor, it was observed that manufacturing operations sequence consists
various forms of non-value-adding activities as follows: (i) The total assembly time for the
Small Electrical Power Screw Air Compressor (SEPSAC) is 236 minutes (ii) Currently the
company is unable to meet the customer demand due to high lead time (iii) Operator
unbalance which increases the man power (iv) The flow of materials from the stores to the
assembly line is not uniform (v) Unwanted movement of people for the search of tools and
equipments and (vi) Inline reworks.
The main goal is to develop different strategies to reduce the level of non value activities
present in any form by implementing the various lean tools. The work targets are given below
and Fig. 1 illustrates the methodology adopted in this work to fulfill the below mentioned
objectives.
To reduce the total assembly time of SEPSAC by 10%.
To identify the bottle neck area in the entire assembly process and overcome with the
help of lean tools and techniques
To do Line balancing with respect to takt time
To streamline the material flow from the stores to the assembly line
To reduce the inline reworks
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Fig. 1 Methodology – Implementation of lean assembly line
4. Implementation and Results
As a first step to establish continuous flow, VSM is done. The current state map [Fig. 2]
presents the existing position of the company. The critical problem areas and different kinds
of non-value added activities are identified in this stage. The next step is development of
future state map. In order to develop the future state map, the current state map was analysed
using the steps and guidelines developed by Rother and Shook [6]. The last step is analysis of
the results obtained after implementing the proposed changes. This has to be quantified in
terms of lead time reduction, cycle time reduction, inventory reduction, etc. Before mapping
the current state it is important to calculate the takt time for the product. The takt time [24
minutes] is the amount of time that must elapse between two consecutive unit completions in
order to meet the demand. It helps to achieve a consistent continuous flow of production
eliminate the waste of over production by producing to actual customer demands.
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Fig. 2 Current state map
From the Current state value stream mapping the time for each stations [Fig. 3] are noted
down. In this work, the focus is on the sub assemblies and the station 1 to station 6. Further,
the total work content analysis of each station in the assembly line with respect to takt time is
noted and given in Fig. 4. It can be noted that the maximum time of the operator is taken as
the station operating time.
Each station with their cycle time and the number of operators working in the respective
stations is given in Table 1. It is noted that the stations 1 and 2 have two operators and the
remaining stations have only one operator each.
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Fig. 3 Station wise operating time
Fig. 4 Work Content analysis
Table 1 Assembly stations with operators and cycle time
Station No of operators Cycle time in minutes
Small parts sub assembly 1 24
Tank sub assembly 1 31
Cooler sub assembly 1 23
Main assembly Station 1 2 25
Main assembly Station 2 2 35
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Main assembly Station 3 1 22
Main assembly Station 4 1 22
Main assembly Station 5 1 22
Main assembly Station 6 1 32
4.1 Kaizen Survey
Kaizen is one of the most important methodologies used to manage continuous improvement
[7]. However, despite the popularity of this philosophy, Kaizen implementations in
companies had little success. So in order to validate kaizen two surveys were conducted with
a list of questionnaire having a set of question and it is distributed among the employees in
the company (SEPSAC Assembly line) with respect to compressors and another one with
respect to general aspects. These studies were conducted with marks maximum of 10. Fig. 5
and 6 represents the kaizen survey with respect to compressors and in general aspects. In the
Fig. 5, the X axis represents the following factors: Creation of screw air compressor
standard document ,factor II - Regular Kaizen identification in the assembly line, factor III -
Identification for tools and fixed point location in the shop floor, factor IV - Standard
operating procedure audit, factor V Visual identification of operator skill level, factor VI -
Implementation of projects from kaizen regularly, factor VII - Rotation plan between the
compressor assembly line to be made and Ensured, factor VIII - Gemba Walk by operation
head, factor IX - Shop standard audit by Engineers, factor X - Parts visibly identified by part
numbers, quantity, and sequence number. Similarly, in the Fig. 6, the following factors
represented: factor XI - Creation of Multi skilling plan for Financial year, factor XII -
Commitment and motivation of staff, factor XIII - Support from senior management, factor
XIV - Allocated resources (time, economic, spaces), factor XV - Developing a culture of
continuous improvement, factor XVI - Set goals for improvement programs, factor XVII -
Using an appropriate methodology, factor XVIII - Standardization and process measurement,
factor X IX - Interdepartmental communication, factor XX - Training and education.
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Fig. 5 Kaizen survey – Compressor specific
Fig. 6 Kaizen survey – Generic in nature
From the survey it is concluded that there is awareness about kaizen in the employees both in
the shop floor and also in office staffs before the commencement of this work. As a result, a
separate plan was prepared especially for kaizen projects and operator skill level. Target dates
are set and persons are allocated the responsibility to meet it. In order to encourage and make
it as a culture in the organization, at the end of every month, from the kaizen list, the best is
selected and implemented. Based on its impact, the concerned worker is awarded with a price.
4.2 Improvements in main assembly station 2
Fig. 7 illustrates the motor and air end subassembly in station 2. First the motor and air end is
shifted to the sub assembly table. Then the intake valve is assembled in the air end followed
by the coupler assembly in motor and air end shaft. Then the hub is assembled in between the
motor and air end. Then at last the discharge control pipe is assembled and the entire sub
assembly is shifted to the main assembly and assembled in the main frame. To identify the
value added and non value added activities in station 2, time study (with stop clock) and
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video study is conducted. It is found that the total time (2100 seconds) consists 1357 seconds
as value added and 743 as non value added. Causes for the non value added time are studied
during the assembly process and also through discussion with the operators. Figure 8
represents the fish bone diagram associated with station 2 and Table 2 shows the kaizen with
respective time reductions. It can be concluded that the kaizen result in significant operating
time reduction i.e. 24 minutes from 35 minutes.
Fig. 7 Motor air end sub assembly
Fig. 8 Station 2: Fish bone diagram
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Table 2 Kaizen: Station 2
Sl No Activity Total time
(Sec)
1 A bin set up can be used such that the operator can place
all the fasteners in the bin at a single time rather than
moving frequently
60
2 Provide the tools in his required position 55
3 The Material trolley should be placed nearer to the sub
assembly table to reduce the movement of the operator
20
4 Adapter ring needs to be grinded 35
5 Check the dimension of the washer. The coupler is a
bought out item so the dimension for the coupler should
be checked with respect to the motor and air end
drawings.
120
6 Torque value for thermal valve tightness should be
checked to avoid bending in the valve
77
7 Instead of entering the details of the motor and air end in
inbuilt card we can go for card(re writable) swiping
250
4.3 Tank sub-assembly - improvements:
The second bottle neck station is tank sub assembly. The assembly process involves in
loading the tank in the assembly fixture with 1253 minutes as value added time and 602
minutes as non value adding. Also, ball valve assembled with the connector and then the top
plate is removed, filter mesh is assembled. Safety valve, oil plug and oil indicator are further
assembled. Once the sub assembly is over then it is moved to main assembly and assembled
in station 2. Like in the previous case, root cause analysis for the tank sub assembly is done
and Fig. 9 gives the Pareto chart. Also kaizen identified (Table 3) results in reduction of non
value added time and the operating time is reduced to 24 minutes.
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Fig. 9 Pareto chart for tank sub assembly
Table 3 Kaizen: Tank sub-assembly
Sl
No
Problem Kaizen Time reduction
(Sec)
1 Movement of the operator for
Searching the fastener and
tool
Provide the fasteners in his
station itself
122
2 Setting of the fixture such
that the tank outlet pipe does
not change its position
Fixture is designed 108
3 Movement of the tank sub
assembly to the station 2
The wheel base in the
trolley can be made
heavier for easy movement
15
4 Operator noting down the
details of the tank in the
inbuilt card
The time can be reduced
by swipe card
70
5 Operator waiting in front of
punching machine.
This process can be shifted
to pre PDI station
130
Total time in seconds 445
5. Summary of Improvements and Conclusion
As a result of implementing kaizen in the bottle-neck stations and reducing the non value
added activities, the total operating time comes below the calculated takt time (Fig 10). Cost-
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benefit analysis (Table 4) reveals substantial cost savings. Further, the total assembly time of
SEPSAC is reduced to 209 minutes from 236 minute (11%). This work gives a set of
alternatives to improve the output of a productive system without incurring in major
investment.
Fig. 10 Station time after improvements
Table 4 Cost benefit analysis
SL No Description Before improvements After
kaizen
1 Cycle time (in minutes) 236 209
2 Cycle time reduction (%) 11
3 Cost of labor per hour Rs.100
4 Total number of labors 11
5 Total cost for labor per day Rs.9900
6 Number of days utilized per
month
21 + 2 (over time) 21
7 Number of days saved 2
8 Cost saved (per month) Rs.19800
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