PowerPD Case Studies Rev 2.6
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Transcript of PowerPD Case Studies Rev 2.6
CASE STUDYCASE STUDY
Latest Case History
PD Test ResultsPD Test Results
Partial Discharge Loose Parts ArcingPartial Discharge, Loose Parts, Arcing
Exact Spot Found
Exact Spot Found
Case Study 2DC transformer # 31@ China@
The mechanical (loose part) signal cannot always make a uniformed signal and does not produce a current. Thus the signal detected from #32 transformer is caused by a loose part that generates arcing (PD)
Loose part on lead connectionLoose part on lead connection
Case Study 3138KV, 100MVA Substation @ Texas, US
This is actual field data from the PD-TP500A. The top screen is Acoustic activity from sensor 2 (Red trace) This shows graphically a real PD repeating pattern. The bottom screen (green trace) is the electrical discharge to ground This is captured via the ‘High Frequency Current Transducer’the electrical discharge to ground. This is captured via the High Frequency Current Transducer
138 KV BUSHING ON PHASE B (PRIMARY) TERMINAL LEADWAS DEFECTED.
138 KV TERMINAL LEAD WAS DEFECTED.
Case Study 4500KV, 1500MVA Substation @ Idaho, US
Transformer; This data collected in June 4, 2007 from the transformer shows a very serious condition coming from outside of transformer, which
has a lot of decrease in the resistance (defective of insulator is high)has a lot of decrease in the resistance (defective of insulator is high).
PD transmits through the air and power line to all grounds of substation equipments.q p
Actual location of PD source
Actual location of PD source
Case Study 566 KV transformer # 2@ India
NDPL in the India, transformer #1 exploded (15 days till testing Tr#2)
66 KV transformer # 1@ India
Transformer; As PD increases, the resistance decreases (defective of insulator is high). Should prepare for the maintenance.
PowerPD was Locate Partial Discharge point using their “PD-TP500A” test device.The location of PD was found within 30 minutes!Th Middl f B h id # 3(Hi h V lt id )The Middle of B phase, side # 3(High Voltage side)
Case Study 6Rotating machine (condensing), US
The data was collected three months before the condensing rotating machine failed
Fault 1 (on “Back end”)
Fault 2 (on “back end”)
Fault 3 (on “front end”)
45 MVA Generator in Thailand
Internal Inspection Findings
??? MVA G t??? MVA Generator in Thailand
15 MVA Generator in Thailand
45 MVA Generator in Thailand
126.6 MVA Generator in ThailandThailand
148 MW Generator in US
Case Study 7PD source from inside of insulation
Internal Inspection Findings
Case Study 8Signal (PD and 6 pulse) was collected from HFCT installed on the tank ground of
Transformer. This signal(PD and 6 pulse) transmitted from the generator side.
6 pulse coming from Generator side
Inspection Findings
Case Study 9Warning level of PD was collected from HFCT installed on the tankWarning level of PD was collected from HFCT installed on the tank ground of Transformer. This PD transmitted from the generator and shot down the generator for maintenanceshot down the generator for maintenance
PD burst collected from HFCT
Inspection Findings
After serviceAfter service
Case Study 10230 KV 300 MVA @ Thailand@
PD burst collected from sensor3(yellow)
Internal Inspection Finding
Case Study 11500 KV 500MVA @ Philippines500 KV 500MVA @ Philippines
PD collected from AE and HFCT
Internal Inspection Finding: Burnt cable from 500kv winding to K pic2 3Burnt cable from 500kv winding to K_pic2.3
Case Study 12 Transformer Test Results:
• TTR Test OK• Doble Test OKDoble Test OK• Doble SFR Test inconclusive• ABB DFR Test:
– Indicates a problem between H&X Winding - Tertiary• Final DGA Test –
Acetylene 3 ppmMethane 1259 ppmEthane 163 ppmEthylene 7 ppmHydrogen 27123 ppm
• ABB Internal Inspection – B phase core shifted due to through f lt / i di t l ifaults/winding telescoping
Transformer test with TP500A @ US
Internal Inspection Findings
E id f h ti b BØ C C li D tEvidence of heating above BØ Core Cooling Ducts
Internal Inspection Findings
Shifted Core over BØ:
Shifted approx ¾” vertically & ½” Horizontally
Case Study 13PD source between winding (Data collected with TP500A)
Internal Inspection Findings
Case Study 14 Transformer Test Results:
• Final DGA TestFinal DGA Test Methane 532 ppmEthane 363 ppmEthane 363 ppmEthylene 13 ppmHydrogen 1,140 ppm (From last year 08 Hydrogen was at 964)y g , pp ( y y g )
PD source from inside of insulation (Data collected with TP500A)
Internal Inspection Findings
Case Study 15 220 KV GIS Test Results: Data collected with iGMS P8220 KV GIS Test Results: Data collected with iGMS_P8
Data from UHF1
Data from UHF2
Data from HFCT
Case Study 16 220 KV GIS Test Results: Data collected with iGMS_P8_
Data from UHF 1 Data from UHF 2 Data from UHF 3 Data from UHF 4