Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation...

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Hoan Bridge Hoan Bridge Failure Analysis Failure Analysis Wisconsin Department of Transportatio City of Milwaukee, WI December 13, 2001 LEHIGH FHWA LICHTENSTEIN

Transcript of Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation...

Page 1: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Hoan BridgeHoan BridgeFailure AnalysisFailure Analysis

Wisconsin Department of TransportationWisconsin Department of Transportation

City of Milwaukee, WIDecember 13, 2001

City of Milwaukee, WIDecember 13, 2001

LEHIGH FHWA LICHTENSTEIN

Page 2: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

OUTLINEOUTLINE Introduction Issues at the Beginning Overview of the forensic

investigation Detailed Analysis Retrofitting of the structure to remain Conclusion

Page 3: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

ISSUESISSUES Secure the area under the failed span Traffic Control and Management What caused the failure Open southbound bridge Repair/Replace existing bridges Follow-up on National Issues

Page 4: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

CAUSES OF FAILURE?CAUSES OF FAILURE? Factors Investigated:

Structural Design of Lateral Brace System Details of Shelf Plate Connection Assembly

(Constraint) Thermal Forces Live Load Forces (Fatigue) Material Properties Weld - Fabrication Quality

Could this have been caught in inspection? Vulnerability of other bridges

Page 5: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

OVERVIEW OF HOAN BRIDGE OVERVIEW OF HOAN BRIDGE FORENSIC INVESTIGATIONFORENSIC INVESTIGATION

Visual Examination Of Fractures Before Demolition Remove Critical Components After Demolition Evaluate Material Properties Global And Local Stress Analysis Of Detail Fractographic And Metallographic Studies Model Crack And Geometric Condition Assess Crack Instability And Arrest

Page 6: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Location F-7View from West

Page 7: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Location E-7View from West

Page 8: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Pier 3S Pier 2SNorth

217-0

24-6

24-6

173-88 Spaces @ 21-8 1/2 = 43-42 Sp. @ 21-8 =

65-1 1/2 108-6 1/2

Girder D

Girder E

Girder F

Floor BeamNumber 1 2 3 4 5 6 7 8 9 10 11

D6 D7 D8

E7

F7

UNIT S2A

F7

Page 9: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Unit S2A Northbound Traffic Lanes East

24-6 24-6

10-012-012-012-06-0

Girder E Girder FGirder D

10-5/16

Page 10: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

WT12X55

WT12X55

WT12X55

WT12X55

1/245deg.

BTC P4E70xx

North

7/8 A-325 Bolts 15/16 Holes (typ.)

Tight Fit

SHELF PLATE DETAIL

LOCATION E-28

Page 11: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

EXTERIOR GIRDER 108G1SECTION F-F

North

WT12X55

WT12X55

1/245deg.

BTC P4E70xx

Page 12: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,
Page 13: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P. 28Shelf Plate Weld Fracture Origin

Crack Origin

Page 14: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P. 28Gusset Plate

Crack OriginCrack Bifurcation

Crack Origin

Page 15: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P. 28Crack Origin

Cleavage Fracture Cleavage Fracture

Page 16: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P. 28Shelf Plate Fracture at Hole Repair

Page 17: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P. 28Shelf Plate Fracture at Hole Repair

Fatigue Striations Ductile Fracture

Surface Abrasion

Page 18: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder E P.P.28Bottom Flange Fracture

Page 19: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder D P.P. 28

Crack OriginsCrack Origins

D 28

Crack Origin

Bottom FlangeCrack Arrest

Page 20: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder D P.P. 28Crack Origins

Cleavage Fracture at Web EdgeCorrosion Pitted Cleavage Fracture

Page 21: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder D P.P.28Bottom Flange

SEM Crack Arrest in Weld HAZ

Page 22: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder D P.P. 28Girder D P.P. 28Crack Arrest in Bottom FlangeCrack Arrest in Bottom Flange

Crack Arrest Boundary

Cleavage Fracture at Crack Tip Cleavage/Ductile Fracture at Crack Tip

Weld

FlangeBase Metal

Page 23: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder B P.P. 26Girder B P.P. 26

Fracture Origins

Page 24: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder B P.P. 26Girder B P.P. 26

Cleavage/Ductile Fracture at Origin Corrosion Product Cleavage Fracture Near Origin

Page 25: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Girder B P.P. 26Girder B P.P. 26Shelf Plate

Web

Thumbnail Defect

Page 26: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

2

2

2

3

3

3

4

4

4

5

5

5

XY

Z

XY

Z

3D Computer Model Of Failed Span/Unit S2a

Page 27: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Finite Element Model Of Joint Assembly

Page 28: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Distance from Joint Center (in)

-12 -10 -8 -6 -4 -2 0 2 4 6 8 10 12 14 16 18 20

Str

ess

(ks

i)

-20-15-10

-505

101520253035404550556065707580

X Normal Elemental StressY Normal Elemental StressZ Normal Elemental Stress

E-28 Stress onWeb Plate

Page 29: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

FRACTURE MODELFRACTURE MODEL

ar

Page 30: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Test Temperature (deg. F)

-120-100 -80 -60 -40 -20 0 20 40 60 80 100 120

CV

N E

nerg

y (f

t-lb)

0

20

40

60

80

100

120

140

E-28 Web Plate

Page 31: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Temperature (deg. F)

-240-210-180-150-120 -90 -60 -30 0 30 60 90 120

KIc (

ksi -

in1/

2)

0

20

40

60

80

100

120

140

160KId Dynamic Load Rate

KIc Static Load Rate

E-28 Web Plate

Page 32: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

EQUIVALENT PENNY SHAPED CRACK

ksiyy 42; t

aK arr 2

sec2

36.1 factorytriaxialit

webenterstipcrackwheninar .5.1

4

5.1sec5.1)3636.1(

2max

xxxK

.127 inksi

.4~2 int

Page 33: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

CRACK ARREST MODELCRACK ARREST MODEL

3/4”

6”

3”

arf

1/2”

1/2”

Page 34: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Temperature (deg. F)

-240-210-180-150-120 -90 -60 -30 0 30 60 90 120

KIc

(ks

i - in

1/2)

0

20

40

60

80

100

120

140

160

KId Dynamic Load Rate

KIc Bridge Load Rate

KId @ NDT

E-28 Flange Plate

Page 35: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,
Page 36: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,
Page 37: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Bracings Disconnected From Shelf Plate

Page 38: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Weigh-in-motion Testing, E. Lincoln Ave. Viaduct

Page 39: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

0

20

40

60

80

100

120

140

0 20 40 60 80 100 120

NUMBER OF TRUCKS

GROSS VEHICLE WEIGHT, Kips

Page 40: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

FINDINGS OF ANALYSIS A Crack-like Geometric Condition Existed At

Intersection Of Shelf Plate And Transverse Connection Plate

Geometry Resulted in High Constraint Stresses From Weight loads And Weld Shrinkage That Were 36% Greater Than Yield Strength Of Material

The Second Retrofit Hole In Center Girder E Increased Stress By 10% At Critical Point

The Bridge Strain Rate Fracture Toughness Of Girder Webs Was 120ksi - , Typical Of A36 Steel Plate

.in

Page 41: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

FINDINGS OF ANALYSIS(continued)

Fracture Was Predicted For The Webs Of All Three Girders; Girder E Started The Failure

Only Girder D Was Capable Of Arresting The Dynamic Crack That Extended To The Flange

Flaws in the Detail Is Not Visually Detected

Page 42: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

FATIGUE-FRACTURE FAILURE OF BRIDGES

Typical progression of failure:

• Micro-discontinuities are present in almost all large fabricated structures, usually in the welds

• With time (and traffic loads), discontinuities could develop into larger fatigue cracks

• It takes many years for fatigue cracks to grow the first few inches ---- normally can be detected visually during field inspections.

• When fatigue cracks reach a critical size, brittle fracture could result (usually on a cold night).

Page 43: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

EFFECT OF CONSTRAINT ON FRACTURE TOUGHNESS

•As constraint is increased, fracture toughness decreases even though the inherent metallurgical characteristics of the steel are not changed

•A triaxial state of stress occurs ahead of the crack which restricts yielding and ductility in the member.

•Constraint (triaxial) played a major role in the fracture at the joints

• Fracture mechanics helps us understand and explain this failure

Page 44: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

RetrofitRetrofitof The Hoan Bridgeof The Hoan Bridge

Approach SpansApproach Spans

Wisconsin Department of TransportationWisconsin Department of Transportation

City of Milwaukee, WICity of Milwaukee, WI

Page 45: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

HOAN BRIDGE RETROFIT

•Removed all lateral bracings

•Removed shelf plates and grind welds smooth and flush with girder webs

•Provided positive attachment between connection plate and tension flange

•Strengthened pier diaphragms for wind forces

•Reconstructed demolished span

Page 46: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

HOAN BRIDGE RETROFIT HIGHLIGHTS

3D Analysis & field test proved bridge can transfer wind loads without lateral bracings.

Performance of retrofit has been field tested

Eliminated fatigue/fracture prone details, driving forces, avoids progressive failure

Future maintenance inspection needs no higher than that for similar steel bridges

Lower cost/completed by year-end

Minimal disruption

Page 47: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,
Page 48: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,
Page 49: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

RETROFITTED SECTION AT INTERIOR

(All Lateral Bracings And Shelf Plates removed)

Page 50: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

RETROFITTED SECTION AT PIER

(Shows strengthening of end diaphragms for wind)

Page 51: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

RECONSTRUCTION OF DEMOLISHED SPAN

•Maintained same superstructure configuration

•Omitted lateral bracings

• Improved girder design to ease fabrication and erection

•Replaced 151 ft section of new girder --- from existing splices

Page 52: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

Conclusions

Location E-7View from West

Cause of failure determined

Replaced demolished span

Removed welded shelf plates

Removed lateral bracings

Strengthening of diaphragms

FINITE ELEMENT MODEL OF JOINT ASSEMBLY

Triaxial Constrained in a critical weld detail is the cause of failure.

Page 53: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

ConclusionsConclusions

Facility service restored andno more problem reported

Continued inspections to monitor potential problems

Promote lessons learned

Page 54: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

National Implications Predictive Models Have

Been Developed

Implemented Cost Effective Rehabilitation Strategies

Heightened Awareness Of Need For Inspections

Education On Use Of The Welded Shelf Plate Detail

FINITE ELEMENT MODEL OF JOINT ASSEMBLY

Page 55: Hoan Bridge Failure Analysis Hoan Bridge Failure Analysis Wisconsin Department of Transportation City of Milwaukee, WI December 13, 2001 City of Milwaukee,

CHALLENGESCHALLENGES How can we improve on the detail (triaxial) Are there better tools to monitor bridges with

this type of detail What would you do differently if you were

called in? What other improvements can be made to the

improved materials (HPS) or fabrication