First Integrated Hydrocracker-DHT unit in ME Its Design ...
Transcript of First Integrated Hydrocracker-DHT unit in ME Its Design ...
First Integrated Hydrocracker-DHT unit in ME –
Its Design, Challenges and Benefits
Talal Al-Rawahi, Orpic
Keshav Nagarhalli, Orpic
Alok Srivastava, ART
Agenda
Introduction to Orpic
Introduction to ART
Integrated Hydrocracker (HCR) - Diesel Hydrotreater (DHT) Unit
in Orpic
HCR in Refinery flow scheme
Orpic HCR configuration
Integrated HCR-DHT advantages
Commissioning challenges
Test run and current performance
Conclusion
Who are we
Orpic is Oman’s national refining and petrochemicals company owned by the
Government of Oman.
Orpic’s Business Model
Orpic Journey
Advanced Refining Technologies (ART)
Who we are
Grace-Chevron joint venture leveraging CLG’s hydrocracking catalyst technology and McDermott's process technology
What we have
A complete portfolio of hydroprocessing catalysts
Substantial resources dedicated to customer support and product development
What we do
Improve the operation and profitability of our customers in the petroleum refining industry
How we do it
Exceptional design of catalyst systems
Fully integrated technical support teams
Why we do it
To provide a single point of contact for
refiners hydroprocessing catalyst needs
Integrated HCR-DHT unit in Orpic
Objective: The objective of the unit is to produce Jet and Ultra Low Sulfur Gasoil product (ULSD) and send Unconverted oil to RFCC
Licensor: Chevron Lummus Global ( CLG)
Unit Configuration:
Hydrocracker ( Isocracking ) unit consists of a two stage hydrocracker (HCR)
integrated with a diesel hydrotreater (DHT).
Total Capacity : 4.055 MMTPA (87,771 BPSD) with turndown at 50% feed rate
HCR I Stage : 2.077 MMTPA (43,043 BPSD)
HCR II Stage : 0.54 MMTPA (11,952 BPSD)
DHT : 1.978 MMTPA ( 44,728 BPSD)
Hydrocracker Conversion – 60 wt.% ( 57 Vol.%), Cycle length – 2 years
The two-stage HCR and DHT share common recycle gas, fractionation, light ends
recovery, LPG treating, fuel gas treating, and make-up hydrogen sections
Integrated HCR-DHT unit in Orpic,
contd.
Unit Feeds:
Hydrocracker section : Designed to process Vacuum gas oil (VGO) from VDU and Heavy Coker Gas Oil (HCGO) from Coker Unit. Straight Run To Cracked Feed Ratio : 75 wt.% : 25 wt.%
Hydrotreating section : Designed to process defined blend of Light Coker Gas Oil (LCGO) from Coker Unit, Heavy Aromatics feed from AOL, Coker Naphtha and Straight run gas oil (SRGO) from CDU. Straight run feed to Cracked Feed Ratio is 51 wt.% : 49 wt.%
Products:
The following major products are produced from the Integrated Hydrocracker Unit:
• Treated Fuel Gas to Header
• Liquefied Petroleum Gas (LPG) to storage
• Light Naphtha to Isom unit
• Heavy Naphtha to AOL
• Jet A-1 to storage
• Diesel with Euro V Specification (<10ppm S) to storage
• Unconverted Oil to RFCC (CCR <0.1Wt%)
YIELDS SOR EOR
Product WT% WT%
H2S 1.72 1.72
NH3 0.14 0.14
C1-C4 1.1 1.39
Light Naphtha 3.45 3.79
Heavy Naphtha 12.42 13.23
Jet A-1 27.15 27.06
Diesel 35.38 34.04
UCO 20.49 20.49
HCR in Refinery Flow Scheme
C4 to LPG Merox
C4
Petroleum
CokeVDU
RFCC
HCR
LPGH N to AOL
JET A1
Diesel
CDU
CDU2
Crude Oil
AR from MAF
BBUBitumen
DCU
HCR Bottom
VGO
VR
CN
LCGO
HCGO
AR
AR
ISOM
L Naphtha
Isomerate
L Naphtha from AOL
Raffinate from AOL
Propylene to OPP
Legend
Existing Units New Units
HA
Integrated HCR-DHT unit in Orpic
Integrated HCR-DHT unit - advantages
Integrating hydroprocessing units saves up to 30% capital cost. Savings are mainly from :
Common Recycle gas and Make Up compressors
Common Fractionation , l ight ends recovery, LPG treating, fuel gas treating systems
Coker Naphtha also processed in DHT section thereby avoiding a Coker Naphtha Hydrotreater
DHT section operates at higher pressures resulting in superior product
quality and longer cycle life
Savings in maintenance and man power costs
Commissioning challenges
Pre-commissioning activities started from July 2017
❖ Catalyst loading done for all three reactors by July
❖ Catalyst wetting and sulphiding done in August
❖ Commissioning of the unit with feed cut-in was done by end August
❖ Performance test run done in December
Challenges faced during commissioning are :
Frequent choking of Amine Filters
Leakage of FT Flanges in HP Loop
High vibrations in Make up gas compressors
LPG Off-spec on Copper corrosion
HP Steam header contamination
Foundation Field Bus issues
Commissioning challenges -
Frequent choking of Amine Filters
Problem
As per design, HCR unit is provided with feed filters in Lean Amine supply line to the unit to remove particulates up to 10 microns. HCR is major consumer of Amine with design flow of 170 m3/h (~65% of total amine circulation)
Post catalyst sulphiding, when HP Amine absorber was taken on line, the amine filters started choking frequently (pressure drop reached limit within 15 mins) making the operation unsustainable and lead to high H2S in Recycle Gas ( up to 2%)
High TSS (above 400 ppm) loading observed in Lean Amine system
Resolution
Rx temperatures were lowered and unit put on long loop circulation @ 50% feed rate and reactor temperatures maintained around 250 oC with 10 m3/h fresh feed to DHT to keep up to 500 ppm H2S in recycle gas system.
Third party temporary filtration skid was installed in the unit with disposable filters. It took more than a week to clean up entire system and establish Amine circulation back to normal values
One of the observation was that during pre-commissioning, each unit amine degreasing was done separately and system did not see full design flowrate.
Commissioning challenges -
Leakages of FT Flanges in HP Loop
Twice unit was shutdown due to leakages resulting in more than 2 weeks downtime
On 25th August , leakage from FT-049 ( II stage treat gas flow orifice ) observed.
Leak was from the spare instrument tapping plug (seal weld).V isual inspection revealed a crack on 1/4th perimeter of the seal welding circumference at the plug.
PMI indicated that the plugs were of Carbon Steel, while they must have been of 1-1/4Cr – 1/2Mo as per Piping Specification
Other Low alloy steel orifice flanges FT’s checked and at total 18 places such anomalies were found. All CS plugs replaced with low alloy F-11 material plugs.
On 16th September, leakage observed on FT-027 ( I stage treat gas flow orifice flange spare plug)
Visual Inspection indicated a crack ¼” above seal welding circumference at the Upper North-East plug
Orifice Flanges related to High Pressure Systems were inspected and those with any issues replaced ( total 59 Plugs replaced)
Issues identified were : Plugs threads not fully engaged, poor quality welding, Small diameter plugs and short length plugs used etc.
Commissioning challenges -
LPG Off-spec on Copper corrosion
Problem
LPG product was going off-spec
on Copper Corrosion since unit commissioning
Unit configuration includes Product
Stripper followed by Fractionator. Feed to Light End Recovery (LER)
section is from Product stripper
overhead and also fractionator overhead.
Troubleshooting actions included : Increasing Temperature profile,
Pressure reduction and purging's
from related columns and frequent caustic replenishments
Resolution
Sampling survey of relevant streams indicated higher H2S slippage from Product Stripper to Fractionator (design < 1ppm slippage). Fractionator overhead naphtha showed high H2S (50-350 ppm).
Licensor was contacted and in house analysis and operating data was shared.
Licensor suggested modification to route fractionator overhead naphtha to Sponge Oil Absorber in LER section to strip off H2S. Earlier this naphtha was fed directly to Debutanizer. Modification was carried out and LPG product came On-Spec after the new line-up was commissioned.
Commissioning challenges -
High vibrations in Make up gas compressors
Problem
High Vibrations observed on
Motor side and on Compressor
Frame
High vibrations are resulting in
foundation getting damaged, bolt loosening, damage to
compressor internals l ike stuffing
box packing and piston ring seals. Instrument tapping also
getting affected. Also crack
found on suction snubber of one compressor.
Resolution
Specialist company hired to study the natural frequencies along with OEM
Counter weights are added as suggested by experts with some respite.
At lower compressor loadings, higher vibrations are observed. So we are forced to run machine at higher loads (less efficient operation). Loading has increased over time to keep vibrations within limit.
Root cause for high vibration is stil l under investigation by vendor.
Commissioning challenges -
HP Steam header contamination
Problem
HP steam header got contaminated asVacuum Distillation (VDU) heateremergency steam to heater pass flowcheck valve was passing and AtmosphericResidue (AR) backed through steam trap tohot clean condensate system. SteamSystem got contaminated with oil for morethan a week before getting noticed.
Boiler feed water contamination withhydrocarbon created excessive foaming inthe steam drum of steam generation systemand led high conductivity water droplets tosteam system passing through demister.Steam turbine blades were fouled due tosteamquality.
Impact was first seen on WGC of DelayedCoker unit and later on RGC inHydrocracker unit. Fouling of HP steamheader led to full opening of governor valveof turbines.
Unit shutdown taken. RGC Turbine openedand fouling observed on rotor blades.
Resolution
Sample result indicated chlorides, piping rustetc. Improper HP Steam Line blowing towardsprocess side was identified as one of the rootcauses.
Turbine blades cleaned by hydroblasting andturbines restarted
Entire steam and condensate systems waspurged to remove trace contaminants andsystem re-established.
Commissioning challenges -
Foundation Field Bus issues
Problem
Control Valves in HCR were opening suddenly and going to their fail safe positions in random fashion.
This happened with approximately 10 control valves including reactor quench control valves
Alert panel engineers took quick action thereby avoiding any upsets and mishaps
Resolution
Problem was identified as
communication failure between DCS and FF Field
instruments
Field barriers firmware changed/upgraded for
120 segments which
appeared suspect
No further problem is
reported since the change.
Test run and current performance
Performance guarantee run and current performance
Unit Performance Guarantee Test Run (PGTR) was done in Dec’17 for a period
of 10 – 12 days after resolving all commissioning issues, in presence of both
CLG and ART personnel
Unit met all the guarantees, viz feed rate, conversion, products yields &
qualities, hydrogen and util ities consumption
Feed properties being monitored closely. Reactor top bed pressure drops are
under control ( less than 1 bar)
Orpic and ART jointly estimating conversion from I and II stage of HCR on weekly basis
Conclusion
Conclusion
Unit is running normal since commissioning
After nearly one year of run length , Catalyst Average Temperatures (CAT) in
reactors are stil l below Start Of Run (SOR)
Unit has been tested on 100% load with higher conversion (65 Vol%) and also
tested at 65% load and 95 Vol% Conversion.
Based on current performance, it will be exceeding 2 years guaranteed
catalyst life. Aim is to extend catalyst life to 4 years to meet turnaround target
with one pit stop for reactor top bed catalyst skimming.
THANKS