DUKE POWER COMPANY · course of a routine maintenance shutdown, a minor system transient occurred,...
Transcript of DUKE POWER COMPANY · course of a routine maintenance shutdown, a minor system transient occurred,...
DUKE POWER COMPANY POWER DUIDIoo
422 SOUTH CHURCH STREET, CHARLOTTE. N C 2e242
WILLIAM 0. PARKER.JR.
VICE PacsorE.T TCLE.ONE: ASA 704
STE.. PpoocT,0 373-083
August 8, 1975
Mr. Norman C. Moseley, Director U. S. Nuclear Regulatory Commission Suite 818 230 Peachtree Street, Northwest Atlanta, Georgia 30303
Re: Oconee Nuclear Station Docket No. 50-287
Dear Mr. Moseley:
My letter of June 27, 1975, transmitted to you Abnormal Occurrence
Report AO-287/75-7, Excessive Reactor Coolant System Cooldown Rate.
The following information provides additional information relating to
this occurrence and associated corrective action.
As stated in AO-287/75-7, when reactor power level had decreased in the
course of a routine maintenance shutdown, a minor system transient
occurred, which resulted in the opening of the power-operated relief
valve 3RC-66. Prior to the system transient, reactor power was being
reduced from 100% FP to 15% FP in an orderly manner by the Integrated
Control System. When 15% FP was reached, unit load demand was 65 Me, and power generation was 115 MWe. This difference between unit load
demand and power generation existed because the reactor was operating
at its low limit of 15% FP while in automatic ICS control and could not
further follow unit load demand. Meanwhile the control operator placed
the turbine control station in manual, leaving the ICS in the "load
tracking" mode. This led to a rapid increase in unit load demand to
match the generated megawatt output. In the meantime, the main steam
bypass valves opened; and when the main steam pressure decreased, the
valves closed. The ICS control of feedwater flow could not follow the
rapid change in unit load demand and steam pressure; consequently,
feedwater flow and steam generator level oscillated, resulting in the
Reactor Coolant System temperature and pressure transient.
The power operated relief valv,,ARC-66, opened when RCS pressure
reached 2255 psi but failed to\elbse when the pressure dropped below
2220 psi, although the open/cl~sed lights in the control room did not
indicate that the valve was opqp. Consequently, RCS pressure dropped,
the reactor tripped on low pre sure, and the HPI system actuated.
79 05lO 3
Mr. Norman C. Moseley Page 2 August 8, 1975
Although the operator closed the isolation valve, 3RC-4, immediately
after the reactor trip to terminate the depressurization, the valve was
reopened because of the rapidly rising pressurizer level. Valve 3RC-4
was finally closed when RC pressure reached 800 psi, terminating the
pressure transient. The subsequent controlled cooldown of the Reactor
Coolant System, when combined with the temperature drop during the
transient, resulted in a cooldown of 1010 F during the first hour when
temperature was below 5300 F, contrary to the provisions of Technical
Specification 3.1.2.3. The transient and associated events also
caused the quench tank rupture disc to blow open, Mirror insulation
to be separated from the bottom nozzle of the pressurizer, and the
release of approximately 1500 gallons of reactor coolant to the Reactor
Building sump.
The release of reactor coolant did not cause any significant increase
of radiation level in the Reactor Building, and no radioactivity was
released into the environment.
As addressed in AO-287/75-7 , the excessive cooldown rate associated with
the transient has been evaluated and it was determined that the health
and safety of the public was not affected. No other system limits were
exceeded.
The failure of 3RC-66 to close and the malfunctioning of the valve
position indication in the Control Room have been investigated. It
has been found that the valve was stuck in the open position because
of heat expansion, boric acid crystal buildup on the valve lever,
rubbing of the level against the solenoid brackets, and bending of
the solenoid spring bracket. The valve was repaired and reinstalled.
The malfunctioning of the valve position indication was not observed
when the repaired valve was reinstalled. This malfunctioning was
apparently caused by the sticking of the solenoid plunger at slightly
less than the full open position or by the crud buildup around the
plunger operated microswitch to the open/closed lights.
Additionally, to prevent recurrence of this incident, the following
corrective actions have been or will be implemented.
1. The unit shutdown procedures for all Oconee units have been revised
to include a change that will prevent decreasing unit load demand
below 120 lIee before placing the ICS in Lhe tcacking mode. This
would minimize the error between the unit load demand and generated
power and thus would reduce the possibility of feedwater flow and
RCS transients.
2. The Units 1 and 2 power-actuated pressurizer relief valves will be
examined as socn as possible for any indication of boric acid
crystal buildup.
Mr. Norman C. Moseley Page 3 August 8, 1975
3. To verify the proper functioning of RC-66, a test to cycle RC-66
prior to startup with a test signal corresponding to 2285 psi will
be incorporated into the station operating procedures.
4. The quench tank rupture disc has been replaced, and the bottom
nozzles on the pressurizer were dye penetrant tested and the
Mirror insulation replaced.
5. Operating personnel have been advised of this incident with specific
instructions that immediate closure of 3RC-4 is the proper corrective
action for such an occurrence.
Ver truly yours,
William 0. Parker, Jr. -j
PMA:vr
cc: Mr. Angelo Giambusso
bcc: Mr. W. S. Lee Mr. S. P. Hellman
Mr. W. H. Owen Mr. H. B. Tucker
Mr. J. E. Smith (15) Mr. G. A. Olson
Mr. J. W. Cox Mr. M. S. Tuckman
Mr. L. Lewis (10) Mr. T. S. Barr
Mr. J. 0. Barbour Mr. R. 0. Sharpe
Mr. K. S. Canady Mr. W. A. Coley
Mr. D. C. Holt Mr. P. M. Abraham
Mr. M. D. McIntosh 1.4.3.5
Mr. P. H. Barton 1.10.3.3
ENCLOSURE 2-2
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ITEM 12
Review your prompt reporting procedures for NRC notification to assure very
early notification of serious events.
Response
The Oconee Nuclear Station Emergency Plan (Station Directive 3.8.5) and the
Administrative Policy Manual for Nuclear Stations (Section 2.8 - Reporting)
include prompt reporting procedures for NRC notification of serious events.
These procedures have been reviewed to assure that the requirements of
10CFR20, 10CFR21, and Oconee Nuclear Station Technical Specification 6.6.2.1.a
(."rompt Notification with Written Followup) are addressed.
Station Directive 3.1.5 (Notification of Station Management) requires prompt
notification of the Operations Unit Coordinator and/or the Station Manager
after any of the following events, among others:
(a) A reactor trip
(b) An unexplained reactivity change
(c) A significant increase in reactor coolant leakage
(d) Loss of offsite power
(e) Major component or equipment failure
(f) Accidental release of liquid or gaseous activity
(g) Known or suspected fuel cladding failure
(h) Suspected initiation of or significant increase in primary-to secondary
leaks
The NRC Resident Inspector and/or the NRC/OIE, Region II, office is to be
notified promptly following determination of any event of regulatory and/or
nuclear safety significance.
DUKE PO- R COMPANY OCONEE UNIT 1
Renort Number: RO-269/782 7
Renort Date: January 15, 1979
Occurrence Date: December 16, 1973
Facility: Oconee Unit 1, Seneca, South Carolina
Identification of Occurrence: ES Actuation Following Reactor Tripo
Conditions Prior to Occurrence: 9P' Full Pcwer
Descri:tion of Occurrence:
A: approxiately 1100 hours cn December 13, 1973, the Reactor Coclan:
System average temperature (Tave) statalarm became erra:ti and a work
recuest to investigate was issued. On December li, 197S during invest
igation of the erratic statalarm behavior a short occurrea cn :ne power
cord feeding the ICS Tave recorder.o The short caused an erroneous 1ow
Tave indizaion of approxi=azaly 13 F. The ICS began wizhdrawing control
rod group 7 to maintain Tave. The reactor tripped on high pressure/temp
erature at 1636 hours. Both normal feedwater pumps tripped on highI
discharge cressure. The emergency.' feedwater pump started, then stop'ped
when the ncrmal feedwater pumps reset and restarted. 3 appro:-:imately
1638 hours :ne level in the OTS's had dropped to 6 andc 0 inches respec
tively (normal level is more than L10 inches). The emergency :eawater
oump started to feed the B generator. Levels in the A ceneracor returned
to normal by 1641 hours but the S generator increased to 35 inches and
then returned to 0. This possibly resulted from malfunctioning of valves
recuired for this particular flow oath. T.-e B genera:ctr as re::iec
thrcugh the emergency feedwater header at 1649 hours. ES Channels 1 and n
(High ?ressure Injection) tripped on low RCS pressure (15C0 psig) as
required by Tecnnical Specifications.
Avoarent Cause of Occurrence:
The ES actuated on low RCS pressure due to ina-ility to maintain feedwa:er
flow to t he OTSG's sufficient to maIntain adequa:e s:ar:uo >eve. .he
feedwa:er problems evident1 resulte: from improper opera:ion of one or
more feedwarer valves (D-AS, -A7) involved in switching o
emer-ency f1cw oaths. The initia:1 grjent, the short in me .averecorders
power cord, was apparently an isola ec,:aJure.
Anal-:s.is of Occurrence:
The heal:h and safety cf the gener 4 uli were not adversely affecte:
as a result of :his occurrence. Sot the RS and ES syscams n
as required.
DUKE P(: ER CCPAN,': OCONEE UNIT i
Pg 2
Corrective Actions:
The power cords that suoply the Tave recorders on Unies 2 and 3 nave been inspected and found to be in accep:able condition.
The potential v malfunctioning valves, FD'- 7, - S will be thoroughly checked during a later outage. Further review of the impac: of zte transient on the OTSG's is also being performed.
N FORM : U. S. NUCLEAR AEGULATCAY CM.misiCN (7-77)
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the power cord suopling the Ta:e recorder shorted caus:ng an a-Darent knot
real) drop in Tave of 13 F. As the ICS a-he=cad to ccree: .2ve ts
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ITEM 3
Review the actions required by your operating procedures for coping with transients
and accidents, with particular attention to:
a. Recognition of the possibility of forming voids in the primary coolant
system large enough to compromise the core cooling capability, espe
cially natural circulation capability.
b. Operator action required to prevent the formation of such voids.
c. Operator action required to ensure continued core cooling in the
event that such voids were formed.
Response
The following emergency procedures have been reviewed and revised to include actions
required to cope with primary coolant system voids:
EP/O/A/1800/0 8 Steam Supply System Rupture
EP/O/A/1800/04 Loss of Reactor Coolant
A graph of the properties of water and saturated steam has been added to the above
listed procedures. The unit computer is available to provide the operator with
saturation temperature versus pressure information. Also, a computer program has
been established to allow the operator to read selected incore thermocouples for
core temperature.
The above procedures have been revised to assure the operator is made aware of:
(a) The possibility of void formation by emphasizing the operator's need
to check for saturation or near saturation conditions in the reactor
coolant system.
(b) The action required to prevent void formation by checking reactor
coolant pressure and temperature following reactor trip to ensure
that there is at least 500F subcooling of the reactor coolant.
(c) The requirement to assure core cooling in the event of void formation
by the operation of at least one reactor coolant pump per loop and the
continuation of HPI operation as described in the response to Item 4.
Operations personnel have been instructed on these procedural changes. Licensed
shift personnel will be sent to the Babcock and Wilcox training simulator, which
has been programmed to demonstrate the events of the Three Mile Island event, for
training expeditiously consistent with scheduling constraints.
ITEM 4
Review the actions directed by the operating procedures and training instructions
to ensure that:
a. Operators do not override automatic actions of engineered safety
features.
b. Operating procedures currently, or are revised to, specify that
if the high pressure injection (HPI) system has been automatically
actuated because of low pressure condition, it must remain in opera
tion until either:
(1) Both low pressure injection (LPI) pumps are in operation
and flowing at a rate in excess of 1000 gpm each and the
situation has been stable for 20 minutes, or
(2) The RPI system has been in operation for 20 minutes, and
all hot and cold leg temperatures are at least 50 degrees
below the saturation temperature for the existing RCS pres
sure. If 50 degree subcooling cannot be maintained after
HPI cutoff, the HPI shall be reactivated.
c. Operating procedures currently, or are revised to, specify that in the
event of HPI initiation, with reactor coolant pumps (RCP) operating,
at least one RCP per loop shall remain operating.
d. Operators are provided additional information and instructions to not
rely upon pressurizer level indication alone, but to also examine
pressurizer pressure and other plant parameter indications in evalua
ting plant conditions, e.g., water inventory in the reactor primary
system.
Response
Operator training includes specific instructions regarding the overriding of auto
matic actions of engineered safety (ES) features. The operators have been in
structed to determine whether or not a valid ES actuation has occurred by verify
ing actual reactor building pressure and reactor coolant system pressure instrumen
tation. If these instruments indicate a valid ES actuation, then the operator is
not to prematurely override the automatic actions. However, if the instruments
indicate a spurious actuation, the operators will take appropriate actions in order
to prevent any damage to the plant that might occur due to this inadvertent actua
tion. Formal briefings on the events at TMI-2 have been held with operations
personnel to assure they are familiar with the events of the incident and proper
methods to cope with the transient. Additional formal training on the proper re
sponse to the events at TMI-2 will be conducted with emphasis placed on the oper
ator's ability to recognize the possibility of void formation and the need to pro
vide adequate core cooling.
ITEM 4 (Continued)
The Emergency Procedures listed in the response to Item 3 have
been revised to
include the specific actions of 4b, c, d above.
Depending upon the nature of the low pressure transient, appropriate operator
action may be required to alter the operation of the high pressure injection
system and/or the reactor coolant pumps in order to prevent an unsafe reactor
coolant system condition.
ITEM 5
Verify that emergency feedwater valves are in the open position in accordance
with Item 8 below. Also, review all safety-related valve positions and posi
tioning requirements to assure that valves are positioned (open or closed) in
a manner to ensure the proper operation of engineered safety features. Also
review related procedures, such as those for maintenance and testing, to ensure
that such valves are returned to their correct positions following necessary
manipulations.
Response
Appropriate feedwater valves have been positioned and visually verified to pro
vice two independent steam generator auxiliary feedwater flow paths. A more
detailed explanation of the actual flow paths is provided in response to Item 8.
Operating procedures for the following systems have been reviewed to assure that
valves are positioned in a manner to assure that engineered safeguards (ES)
systems and related equipment can perform their intended functions:
Emergency Feedwater System
High Pressure Injection System Reactor Building Spray System Low Pressure Injection System Reactor Building Cooling System Penetration Room Ventilation System Core Flooding System Valves Associated with Containment Isolation Function
Operating procedure OP/O/A/1102/06, Removal and Restoration of Station Equipment,
establishes the methods to be used to remove station equipment from service or to
change its status as required by another operating procedure. Requirements are
included to provide documentation of sufficient testing to assure that the equip
ment is fully operable prior to returning the equipment to service. This proce
dure also provides steps to identify any equipment that is inoperable, out of
specification or does not otherwise meet necessary operational requirements.
Procedures applicable to maintenance and periodic testing have been reviewed and
verified to include provisions to assure that all components, including valves,
are returned properly to service following maintenance or testing. The following
procedures have been revised:
IP/O/A/0310/7B ES Logic Subsystem, 1LPI, CH-3
IP/O/A/0310/7C ES Logic Subsystem, 1RB Isolation, CH-5
IP/0/A/0310/8C ES Logic Subsystem, 2RB Isolation, CH-6
IP/O/A/0310/15 RB Pneumatic Isolation Valve Check
IP/O/A/0310/17 PM of Quick Exhaust Valves on PR-2, -3, -4,
0 ITEM 6
Review the containment isolation initiation design and procedures and prepare
and implement all changes necessary to cause containment isolation of
all lines
whose isolation does not degrade core cooling capability upon automatic initia
tion of safety injection.
Response
All containment isolation valves with the exception of the following are normally
closed during operation and receive a close signal upon activation
of containment
isolation at a Reactor Building pressure of 4 psig:
(a) Pressurizer sample lines (1/2") are kept open to facilitate routine sampling.
(b) The low pressure service water to the reactor coolant pump motors
and component
cooling water to the reactor coolant pump seals are open. Closure of valves
in these systems could result in the reactor coolant pumps being
inoperable.
Such a condition is not considered generally desirable and is not consistent
with other portions of E Bulletin 79-O5A covering RCP operation for core
cooling capability.
No changes are deemed necessary to the containment isolation system design or
operation.
ITEM 7
For manual valves or manually-operated motor-driven valves which could defeat
or compromise the flow of auxiliary feedwater to the steam generators, pre
pare and implement procedures which:
(a) require that such valves be locked in their correct position, or
(b) require other similar positive position controls.
Response
The response to this item will be provided by April 16, 1979.
ITEM 8
Prepare and implement immediately procedures which assure that two independent
steam generator auxiliary feedwater flow paths, each with 100% flow capacity,
are operable at any time when heat removal from the primary system is
through the steam generators. When two independent 100% capacity flow paths
are not available, the capacity shall be restored within 72 hours or the
plant shall be placed in a cooling mode which does not rely on steam
generators for cooling within the next 12 hours.
When at least one 100% capacity flow path is not available, the reactor
shall be made subcritical within one hour and the facility placed in a
shutdown cooling mode which does not rely on steam generators for cooling
-rithin 12 hours or at the maximum safe shutdown rate.
Response
The response to this item will be provided by April 16, 1979.
ITEM 9
Review your operating modes and procedures for all systems designed to transfer
potentially radioactive gases and liquids out of the primary containment to
assure that undesired pumping of radioactive liquids and gases will not occur
inadvertently.
In particular, ensure that such an occurrence would not be caused by the resetting
of engineered safety features instrumentation. List all such systems and indicate:
a. Whether interlocks exist to prevent transfer when high radiation
indication exists, and
b. Whether such systems are isolated by the containment isolation signal.
Response
The following systems have the capability to transfer potentially radioactive
gases and liquids out of containment:
(a) Reactor Building normal sump to the miscellaneous waste holdup tank
(liquid) (b) Reactor Building emergency sump to the high activity waste tank (liquid)
(c) Reactor Building purge to the unit vent (gaseous)
(d) Gaseous waste disposal system (gaseous)
(e) Quench Tank drain system
The only system in which automatic actuation is a design feature is (a) above.
The pumps in this system have the capability to start automatically when sump
level is high and pump liquid to the miscellaneous holdup tank. However, operating
procedures require that this system be operated manually and a modification is in
process to remove this capability. The remaining systems are all operated manually,
with operator actuation required to align the system for transfer and then to
initiate transfer.
An interlock exists between the Reactor Building gas monitor
and Reactor Building
normal sump pump to prevent transfer in the event of high gaseous activity.
An interlock also exists between the unit vent gas monitor and Reactor Building
purge to secure the purge in the event of high gaseous activity in the unit vent.
All of these systems are isolated by the containment isolation signal. Upon re
setting of the containment isolation signal, all valves remain closed. Operator
action is required to reposition any containment isolation valve.
ITEM 10
Review and modify as necessary your maintenance and test procedures to ensure
that they require:
(a) Verification, by inspection, of the operability of redundant safety
related systems prior to the removal of any safety-related system from
service.
(b) Verification of the operability of all safety-related systems when they
are returned to service following maintenance or testing.
(c) A means of notifying involved reactor operating personnel whenever a
safety-related system is removed from and returned to service.
Response
The response to this item will be provided by April 16, 1979.
ITEM 11
All operating and maintenance personnel should be made aware of the extreme
seriousness and consequences of the simultaneous blocking of both auxiliary
feedwater trains at the Three Mile Island Unit 2 plant and other actions
taken during the early phases of the accident.
Response
The response to this item will be provided by April 16, 1979.