Daily Elect Report Feb'12

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Da Date Faults 01.02.12 AF comp. L1 paramix Alarm saving problem 02.02.12 L1 paramix Alarm saving problem L1 filler Valve not opend ETP Blower motor not run 04.02.12 GRB Conveyer Conveyer modification Padovan CIP AF comp. ADT control card burnt Date code m/c 06.02.12 Unicorn CIP CO2 Plant 07.02.12 L1 paramix Syrup pump tripped Submersible pump Send for servicing L3 conveyer Blower Sensor installation Balast & switch burnt FSR return pump L-2 video jet Bad Printing quality Machine name/Place CIP caustic transfer pump Motor tripped.Water found inside the motor due to seal leakage. Compressor tripped.Drier ADT control card burnt. Mixture ratio range problem Anton paar CO2 volume problem Mixture ratio range problem Anton paar CO2 volume problem Solenoied valve not open Sensor didn’t sence the new crown Caustic concentrate inside the pipe & caustic drum Level fluctuation problem L3 bent tube detector L-2 bottle inspection shed Motor tripped.Water found inside the motor due to seal leakage. L-3 C/C buffer tank CO2 line solenoid valve not open

Transcript of Daily Elect Report Feb'12

Page 1: Daily Elect Report Feb'12

Daily Electrical Report (FEB'2012)

Date Faults

01.02.12AF comp.

L1 paramix

Mixture ratio range problem

Alarm saving problem

02.02.12

L1 paramix

Mixture ratio range problem

Alarm saving problemL1 filler Valve not opend

ETP Blower motor not run

04.02.12

GRB Conveyer Conveyer modification

Padovan CIP Solenoied valve not open AF comp. ADT control card burnt

Date code m/c

06.02.12Unicorn CIP

CO2 Plant Level fluctuation problem

07.02.12

L1 paramix Syrup pump tripped

Submersible pump Send for servicing

L3 conveyer Blower

Sensor installation

Balast & switch burnt

FSR return pump

L-2 video jet Bad Printing quality

L-3 C/C buffer tank

Machine name/Place

CIP caustic transfer pump

Motor tripped.Water found inside the motor due to seal leakage.Compressor tripped.Drier ADT control card burnt.

Anton paar CO2 volume problem

Anton paar CO2 volume problem

Sensor didn’t sence the new crown

Caustic concentrate inside the pipe & caustic drum

L3 bent tube detector L-2 bottle inspection shed

Motor tripped.Water found inside the motor due to seal leakage.

CO2 line solenoid valve not open

Page 2: Daily Elect Report Feb'12

07.02.12

L-3 SMI

08.02.12

L-3 Alpha Jet Bad Printing quality

Auto clave servicing

Husky Plant

09.02.12

L-1 Shrink wrapper Panel A/C servicingAuto clave servicing

AF comp. ADT tripped

L-3 Alpha Jet Bad Printing quality

11.02.12

Shrink film plant Lighting

12.02.12

L4 date coding

switch problem

Old pump is not sufficient

L3 warmer MPCB problem

Syrup room AC problem

Installation

IR dryer

AF comp.(860) Water pump tripped

13.02.12

Syrup room AC problem

Pump no.-11 & 25 not run

IR dryer

Machine tripped showing Masssage "general Shut down."

Piovan Chiller tripped due to temp sensor problem.

Husky Submersible pump

New submersible pump start frequently due to low reservationL402 (Imaje 9040) not print. Ink come outside of the gutter

L2 filler inspection shadeHusky Submersible pump

L-3 vent tube detector

L1 filler capper hopper

capper hopper motor not run correctly due to sensor adjustment.Refregerent gas pressure low

Water treatment plant

Refregerent gas pressure low

Page 3: Daily Elect Report Feb'12

13.02.12

QC lab Incubetor servicing

Substation ETP breaker installation

Installation

14.02.12

L4 date coding

Supply pressure reduce

QC lab Incubetar servicing

15.02.12

L-1 tunnel Heater Cooling fan installationFM room A/C power socket burntETP plant Lighting

WTP Water heater

Pump House Pump-15 tripped

RM store Lighting

L-1 tunnel Heater Heater problem

Sugar conveyer Celing fan problem

AC problem

16.02.12

L4 date coding

L4 conveyer

AC problem

QC lab Incubater

Online UPS New Battery Installation

18.02.12

Workshop

L-1 tunnel Heater Heater problem

L-3 vent tube detector

New Imaje 9030 date code machine installation

L2 Carbocooler buffer tank

Solenoid valve malfunctioning

Cooline chiller pump

Finished Syrup Room

Imaje 9040 tripped showing "Gutter recuparation fault"

Motor didn’t run due to conveyer displacement

Finished Syrup Room

Welding machine power card problem

Page 4: Daily Elect Report Feb'12

18.02.12 L-4 Imaje 9040 Ink came outside the gutter

QC lab IncubatorUnicorn CIP Agitator Motor not run

Coil damaged

19.02.12

Installation

switch problem

Raw Syrup Room Cable dresingWTP Pump no.-11 not runSMI Output chain drive stoppedFM room A/C power socket burntFSR Room A/C servicing

20.02.12L-2 pasturizer

L-2 celing fan Not run

22.2.12

L-3 Labeller Panel AC tripped

Cable installation

UPS Not charged

L-1 warmer

L-1 tunnel Heater Heater problem

LP comp. Maintenance

23.02.13

Imaje 9040 Hired machine

L-2 Carbocooler Water level sensor problem

Online UPS Charging problemIR compresser Maintenance

GRB flow mix pump motor

L-2 vent tube detectorL-2 inspection shade

Solenoid valve not work in auto mode

L-3 vent tube detector

Temperatur controller installation

Page 5: Daily Elect Report Feb'12

Daily Electrical Report (FEB'2012)

Job Description Present status

Take out the defective ADT.

KHS expert NEO is trying to solve these problem. Continue..

Neo cant increase the mixture ratio range.

Now its working good.

Modify the program. Now alarm is saved.checked & changed one 24dc solenoied. Solved

Solved

Replaced the defective solenoied card. SolvedReplaced the defective ADT. Solved

Solved

Solved

Solved

Solved

Take out the blower from line-3. Done

Sensor installation & wiring is going on.

Replaced the shade. Repaired the burnt shade with new wiring. Solved

Solved

Wash the head & adjust the sensor & head. Ok.

Checked coil & valve, cleaned plunger. Solved

Dismantle the motor,checked coil & found ok. Changed the seal, heated the armature & refited. No load current-3.1,3.1,3.2 (Rated current-5.5A)

This comp. is not in service now.

There is leakage inside the anton paar CO2 measuring module. Changed 3 pcs diaphragms.

Checked & changed defective auxiliary contact. Rated current-2.8A, Running current-2.2APrepared one new Control box.Installed new cable tray, control panel & connected the motor with control panel.

Adjust the sensor & bring a new optical fiber photo sensor adapter for high speed printing at L4.

Dismantle caustic dosing pump, pipe line & clean the caustic solution drum by hot water. After cleaning the whole dosing system dosing has been run automatically. Connect the agitator motor.

Tried to stable the re-boiler by changing some PID value of Lean MEA & rich MEA pump but no improvement.

Need to consult with expert.

Checked the motor & control circuit. Magnetic contactor sizzed. Made it free & run the motor.Installed the pump, Checked & connected the motor. Insulation resistance-200Mohm(p-p), 100Mohm(p-b).

Replaced the motor. Dismantle the motor,checked coil & found ok. Changed the seal, heated the armature, refited.

Page 6: Daily Elect Report Feb'12

solved

Checked & temperory manage to run the chiller.

Installed the old panel A/C into shrink wrapper machine. Ok.After servicing, handed over the auto clave to QC department. Ok.

Now it is running

Installed 2 nos. metal halide lamp at shrink film plant. Complete

Now old one is running.

Need to call expert.

replaced the toggle switch. Ok.

Again connect the new pump. Under observation

MPCB was under rated. Replaced the defective MPCB. Ok.

Ok.

Continue..

Adjust the sensor & increase the time in timer. solved

Third party checheked for leakage. Continue..

solved

Ok.

solved

Charged refregerant as they found no leakage. Now it is running. Under observation

Checked all control circuit, communication cable & found a fuse burnt inside optical communication module. Changed the burnt fuse.

Solved. Now machine is running.

Expert checked the machine, changed the motherboard but found no improvement. Now the machine is running on "Auto Refresh" mode. Printing is done by Imaje 9030.

This machine is under maintenance.

Heater is checked by connecting 2 pin power socket. Coil is ok but found water leakage with heater connection.

Need to purchase a new sensor

Took apart the ADT and checked for leakage but ok. Reset the ADT & run the comp.Expert again checked the machine and suggested to changed the ink tank.

This machine is now running.

Disconnected the new pump and set back the pressure switch connection to old pump.

Contact with imaje expert and carried out the suggested procedure several times. But no improvement.

Checked all AC & tried to repair one today. Changed compressor, refregerant gas.Wirinig and sensor installation completed. But could not connect emergency switch connection as line was running.

Checked motor connection & found defective magnetic contactor. Replaced the defective magnetic contactor

3 Nos. AC servicing completed. Replaced 2 compressor, charged refregent in one compressor & clean outdoor, indoor unit.

Run the alternate pump-10 first then checked control circuit & adjust the float switch.Production stopped 15 mins due to this problem.

Page 7: Daily Elect Report Feb'12

Continue..

Made copper bar for 300A MCCB terminal connection. Continue..

Need CIP to connect the sensors with existing control circuit. Continue..

Now kept as stand by.

Checked & servicing carried out of the solenoid valve. Ok.

solved

Need to consult with EM.

installed two metal body cooling fan on L-1 heater. Ok.replaced the power socket. Ok.Connected two 200W incandicent bulb. Ok.

Checked 7 found one heater coil burnt.

RM store lighting is going on. Need more tubelight shade. Continue..

Continue..

Repaired one & set it back. Ok.

Continue..

Wash the head & reset the fault. Kept as stand by

After adjusting the conveyor, run the motor solved

Checked AC-2 & found leakage. Trying to replace the outdoor unit. Continue..

Continue..

Installed 96 pcs new battery in 40 KVA online UPS.

Checked & found dry soldering. Carried out solderring properly. solved

Checked control circuit & found burnt temperature controller in one machine. Trying to service this controller. Other machine has control card problem (could not get nutral connection). Trying to solve this problem.

A new Imaje 9030 date code machine has been installed for high speed printing at L-4.

Supply pressure reduced to 1-1.5 bar due air problem at sucktion line. Made the pump air free. Motor rated current 10A, now running current 5.5A & pressure 6 bar

Checked all control circuit but could not possible to run the machine correctly. This machine can be modified by using a temperature controller & solied state relay to control the temperature.

Other two are heating now.

tripped due to pump side jamming. Mechanical servicing carried out. Now the motor takes normal running current.

First changed the power cable. But after few hours heater burnt. Need to find the problem during CIP. Now it heated by other two coil.

Repaired leakage of AC-5, vaccumed & charged refregernt gas. Also charged refregerent gas into AC-3.

Modification work going on.One of the circuit is replaced by temperature controller, magnetic contactor & a thermocouple.

Need to checked by expert

Take out the heater box, Checked coil resistance & found 23ohms at both coil. But insulation resistance differ. So, refited the good one. Another coil was kept at tools room as it sparked.

Need to find out the cause during CIP.

Page 8: Daily Elect Report Feb'12

Cleaned the head & kept it as stand by. ok

Repaired one machine & sent it to QC lab for their observation. Under observationOverload relay found faulty. Changed the overload relay. solved

Installed one more relay & reset switch & completed wiring.

Give direct connection as new switch was not available.

Carried out cable dressing at raw syrup room. okChecked & found problem in float switch. Servicing carried out. ok.Reset the drive. okReplaced the power socket with a breaker. okSolved the leakage problem of FSR A/C-2. ok

As production started, so ran it manualy.

Checked & found the coil burnt.

AC tripped due to air block. Clean the AC carefully. ok

Replaced 3 core wire by 4 core for DC nutral. ok

Checked and found that charging card still faulty. Need to repair.

Continue..

Replaced the coil. solved

ok

Sent back the hired machine. ok

Checked & found loose contact of the level sensor. ok

Checked by third party. Didn’t find out the problem. Not solvedClean the panel, checked & tightened all the connection ok

Rewinding completed, varnished the coil, Checked coil resistance & found 2.3ohms from each coil. Assambled & ran the motor. Motor vibrate & made abnormal sound.

Need to contact with rewinding party.

Need CIP to adjust the sensorNeed to change the switch

Need to find out the cause during CIP.Need to install another fan

Prepared the controller for installation. It t will be installed during CIP.

Clean the panel, checked & tightened all the connection. Servicing carried out of a solenoid valve.

Page 9: Daily Elect Report Feb'12

Daily Electrical Report (FEB'2012)

Work done by

Page 10: Daily Elect Report Feb'12

Manik,Matin

Third party, Nur Alam

Shahnuzzaman, Matin

Page 11: Daily Elect Report Feb'12

Sharif, Barun

Manik

Sharif, Barun

Habib

Shahnuzzaman, Matin

Shahnuzzaman, Matin

Sharif, AnisMahfuz, AnisManiruzzamanAnis, Barun

Mahfuz

Mahfuz, BarunKhokon

Latif, Ripon

Barun

Maniruzzaman

matin

Maniruzzaman

Sharif, Anis

Anis, Barun

Anis

Mahfuz, Barun

Shahnuzzaman, Matin

Page 12: Daily Elect Report Feb'12

Habib

SharifSharif, Barun

Shanuzzaman, Matin

Sharif

Habib, Ripon

Sharif, RiponHabibShahnuzzamanManiruzzamanManiruzzaman

Mahfuz, anis

Mahfuz, Anis

Maniruzzaman

Sharif

Sharif

habib

habib

Barun

anis

Third party, SharifManik,Latif