Daily Elect Report Feb'12
Transcript of Daily Elect Report Feb'12
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Daily Electrical Report (FEB'2012)
Date Faults
01.02.12AF comp.
L1 paramix
Mixture ratio range problem
Alarm saving problem
02.02.12
L1 paramix
Mixture ratio range problem
Alarm saving problemL1 filler Valve not opend
ETP Blower motor not run
04.02.12
GRB Conveyer Conveyer modification
Padovan CIP Solenoied valve not open AF comp. ADT control card burnt
Date code m/c
06.02.12Unicorn CIP
CO2 Plant Level fluctuation problem
07.02.12
L1 paramix Syrup pump tripped
Submersible pump Send for servicing
L3 conveyer Blower
Sensor installation
Balast & switch burnt
FSR return pump
L-2 video jet Bad Printing quality
L-3 C/C buffer tank
Machine name/Place
CIP caustic transfer pump
Motor tripped.Water found inside the motor due to seal leakage.Compressor tripped.Drier ADT control card burnt.
Anton paar CO2 volume problem
Anton paar CO2 volume problem
Sensor didn’t sence the new crown
Caustic concentrate inside the pipe & caustic drum
L3 bent tube detector L-2 bottle inspection shed
Motor tripped.Water found inside the motor due to seal leakage.
CO2 line solenoid valve not open
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07.02.12
L-3 SMI
08.02.12
L-3 Alpha Jet Bad Printing quality
Auto clave servicing
Husky Plant
09.02.12
L-1 Shrink wrapper Panel A/C servicingAuto clave servicing
AF comp. ADT tripped
L-3 Alpha Jet Bad Printing quality
11.02.12
Shrink film plant Lighting
12.02.12
L4 date coding
switch problem
Old pump is not sufficient
L3 warmer MPCB problem
Syrup room AC problem
Installation
IR dryer
AF comp.(860) Water pump tripped
13.02.12
Syrup room AC problem
Pump no.-11 & 25 not run
IR dryer
Machine tripped showing Masssage "general Shut down."
Piovan Chiller tripped due to temp sensor problem.
Husky Submersible pump
New submersible pump start frequently due to low reservationL402 (Imaje 9040) not print. Ink come outside of the gutter
L2 filler inspection shadeHusky Submersible pump
L-3 vent tube detector
L1 filler capper hopper
capper hopper motor not run correctly due to sensor adjustment.Refregerent gas pressure low
Water treatment plant
Refregerent gas pressure low
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13.02.12
QC lab Incubetor servicing
Substation ETP breaker installation
Installation
14.02.12
L4 date coding
Supply pressure reduce
QC lab Incubetar servicing
15.02.12
L-1 tunnel Heater Cooling fan installationFM room A/C power socket burntETP plant Lighting
WTP Water heater
Pump House Pump-15 tripped
RM store Lighting
L-1 tunnel Heater Heater problem
Sugar conveyer Celing fan problem
AC problem
16.02.12
L4 date coding
L4 conveyer
AC problem
QC lab Incubater
Online UPS New Battery Installation
18.02.12
Workshop
L-1 tunnel Heater Heater problem
L-3 vent tube detector
New Imaje 9030 date code machine installation
L2 Carbocooler buffer tank
Solenoid valve malfunctioning
Cooline chiller pump
Finished Syrup Room
Imaje 9040 tripped showing "Gutter recuparation fault"
Motor didn’t run due to conveyer displacement
Finished Syrup Room
Welding machine power card problem
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18.02.12 L-4 Imaje 9040 Ink came outside the gutter
QC lab IncubatorUnicorn CIP Agitator Motor not run
Coil damaged
19.02.12
Installation
switch problem
Raw Syrup Room Cable dresingWTP Pump no.-11 not runSMI Output chain drive stoppedFM room A/C power socket burntFSR Room A/C servicing
20.02.12L-2 pasturizer
L-2 celing fan Not run
22.2.12
L-3 Labeller Panel AC tripped
Cable installation
UPS Not charged
L-1 warmer
L-1 tunnel Heater Heater problem
LP comp. Maintenance
23.02.13
Imaje 9040 Hired machine
L-2 Carbocooler Water level sensor problem
Online UPS Charging problemIR compresser Maintenance
GRB flow mix pump motor
L-2 vent tube detectorL-2 inspection shade
Solenoid valve not work in auto mode
L-3 vent tube detector
Temperatur controller installation
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Daily Electrical Report (FEB'2012)
Job Description Present status
Take out the defective ADT.
KHS expert NEO is trying to solve these problem. Continue..
Neo cant increase the mixture ratio range.
Now its working good.
Modify the program. Now alarm is saved.checked & changed one 24dc solenoied. Solved
Solved
Replaced the defective solenoied card. SolvedReplaced the defective ADT. Solved
Solved
Solved
Solved
Solved
Take out the blower from line-3. Done
Sensor installation & wiring is going on.
Replaced the shade. Repaired the burnt shade with new wiring. Solved
Solved
Wash the head & adjust the sensor & head. Ok.
Checked coil & valve, cleaned plunger. Solved
Dismantle the motor,checked coil & found ok. Changed the seal, heated the armature & refited. No load current-3.1,3.1,3.2 (Rated current-5.5A)
This comp. is not in service now.
There is leakage inside the anton paar CO2 measuring module. Changed 3 pcs diaphragms.
Checked & changed defective auxiliary contact. Rated current-2.8A, Running current-2.2APrepared one new Control box.Installed new cable tray, control panel & connected the motor with control panel.
Adjust the sensor & bring a new optical fiber photo sensor adapter for high speed printing at L4.
Dismantle caustic dosing pump, pipe line & clean the caustic solution drum by hot water. After cleaning the whole dosing system dosing has been run automatically. Connect the agitator motor.
Tried to stable the re-boiler by changing some PID value of Lean MEA & rich MEA pump but no improvement.
Need to consult with expert.
Checked the motor & control circuit. Magnetic contactor sizzed. Made it free & run the motor.Installed the pump, Checked & connected the motor. Insulation resistance-200Mohm(p-p), 100Mohm(p-b).
Replaced the motor. Dismantle the motor,checked coil & found ok. Changed the seal, heated the armature, refited.
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solved
Checked & temperory manage to run the chiller.
Installed the old panel A/C into shrink wrapper machine. Ok.After servicing, handed over the auto clave to QC department. Ok.
Now it is running
Installed 2 nos. metal halide lamp at shrink film plant. Complete
Now old one is running.
Need to call expert.
replaced the toggle switch. Ok.
Again connect the new pump. Under observation
MPCB was under rated. Replaced the defective MPCB. Ok.
Ok.
Continue..
Adjust the sensor & increase the time in timer. solved
Third party checheked for leakage. Continue..
solved
Ok.
solved
Charged refregerant as they found no leakage. Now it is running. Under observation
Checked all control circuit, communication cable & found a fuse burnt inside optical communication module. Changed the burnt fuse.
Solved. Now machine is running.
Expert checked the machine, changed the motherboard but found no improvement. Now the machine is running on "Auto Refresh" mode. Printing is done by Imaje 9030.
This machine is under maintenance.
Heater is checked by connecting 2 pin power socket. Coil is ok but found water leakage with heater connection.
Need to purchase a new sensor
Took apart the ADT and checked for leakage but ok. Reset the ADT & run the comp.Expert again checked the machine and suggested to changed the ink tank.
This machine is now running.
Disconnected the new pump and set back the pressure switch connection to old pump.
Contact with imaje expert and carried out the suggested procedure several times. But no improvement.
Checked all AC & tried to repair one today. Changed compressor, refregerant gas.Wirinig and sensor installation completed. But could not connect emergency switch connection as line was running.
Checked motor connection & found defective magnetic contactor. Replaced the defective magnetic contactor
3 Nos. AC servicing completed. Replaced 2 compressor, charged refregent in one compressor & clean outdoor, indoor unit.
Run the alternate pump-10 first then checked control circuit & adjust the float switch.Production stopped 15 mins due to this problem.
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Continue..
Made copper bar for 300A MCCB terminal connection. Continue..
Need CIP to connect the sensors with existing control circuit. Continue..
Now kept as stand by.
Checked & servicing carried out of the solenoid valve. Ok.
solved
Need to consult with EM.
installed two metal body cooling fan on L-1 heater. Ok.replaced the power socket. Ok.Connected two 200W incandicent bulb. Ok.
Checked 7 found one heater coil burnt.
RM store lighting is going on. Need more tubelight shade. Continue..
Continue..
Repaired one & set it back. Ok.
Continue..
Wash the head & reset the fault. Kept as stand by
After adjusting the conveyor, run the motor solved
Checked AC-2 & found leakage. Trying to replace the outdoor unit. Continue..
Continue..
Installed 96 pcs new battery in 40 KVA online UPS.
Checked & found dry soldering. Carried out solderring properly. solved
Checked control circuit & found burnt temperature controller in one machine. Trying to service this controller. Other machine has control card problem (could not get nutral connection). Trying to solve this problem.
A new Imaje 9030 date code machine has been installed for high speed printing at L-4.
Supply pressure reduced to 1-1.5 bar due air problem at sucktion line. Made the pump air free. Motor rated current 10A, now running current 5.5A & pressure 6 bar
Checked all control circuit but could not possible to run the machine correctly. This machine can be modified by using a temperature controller & solied state relay to control the temperature.
Other two are heating now.
tripped due to pump side jamming. Mechanical servicing carried out. Now the motor takes normal running current.
First changed the power cable. But after few hours heater burnt. Need to find the problem during CIP. Now it heated by other two coil.
Repaired leakage of AC-5, vaccumed & charged refregernt gas. Also charged refregerent gas into AC-3.
Modification work going on.One of the circuit is replaced by temperature controller, magnetic contactor & a thermocouple.
Need to checked by expert
Take out the heater box, Checked coil resistance & found 23ohms at both coil. But insulation resistance differ. So, refited the good one. Another coil was kept at tools room as it sparked.
Need to find out the cause during CIP.
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Cleaned the head & kept it as stand by. ok
Repaired one machine & sent it to QC lab for their observation. Under observationOverload relay found faulty. Changed the overload relay. solved
Installed one more relay & reset switch & completed wiring.
Give direct connection as new switch was not available.
Carried out cable dressing at raw syrup room. okChecked & found problem in float switch. Servicing carried out. ok.Reset the drive. okReplaced the power socket with a breaker. okSolved the leakage problem of FSR A/C-2. ok
As production started, so ran it manualy.
Checked & found the coil burnt.
AC tripped due to air block. Clean the AC carefully. ok
Replaced 3 core wire by 4 core for DC nutral. ok
Checked and found that charging card still faulty. Need to repair.
Continue..
Replaced the coil. solved
ok
Sent back the hired machine. ok
Checked & found loose contact of the level sensor. ok
Checked by third party. Didn’t find out the problem. Not solvedClean the panel, checked & tightened all the connection ok
Rewinding completed, varnished the coil, Checked coil resistance & found 2.3ohms from each coil. Assambled & ran the motor. Motor vibrate & made abnormal sound.
Need to contact with rewinding party.
Need CIP to adjust the sensorNeed to change the switch
Need to find out the cause during CIP.Need to install another fan
Prepared the controller for installation. It t will be installed during CIP.
Clean the panel, checked & tightened all the connection. Servicing carried out of a solenoid valve.
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Daily Electrical Report (FEB'2012)
Work done by
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Manik,Matin
Third party, Nur Alam
Shahnuzzaman, Matin
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Sharif, Barun
Manik
Sharif, Barun
Habib
Shahnuzzaman, Matin
Shahnuzzaman, Matin
Sharif, AnisMahfuz, AnisManiruzzamanAnis, Barun
Mahfuz
Mahfuz, BarunKhokon
Latif, Ripon
Barun
Maniruzzaman
matin
Maniruzzaman
Sharif, Anis
Anis, Barun
Anis
Mahfuz, Barun
Shahnuzzaman, Matin
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Habib
SharifSharif, Barun
Shanuzzaman, Matin
Sharif
Habib, Ripon
Sharif, RiponHabibShahnuzzamanManiruzzamanManiruzzaman
Mahfuz, anis
Mahfuz, Anis
Maniruzzaman
Sharif
Sharif
habib
habib
Barun
anis
Third party, SharifManik,Latif