Ammonia CW Case Study 08 Feb 06
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Transcript of Ammonia CW Case Study 08 Feb 06
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Cooling Water Treatment
-An Experience at GNFC
By N. B. Bhatt and A.M. Vashi
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GNFC AT A GLANCE
Incorporation : May10,1976
Capacity Per Annum Ammonia : 4,45,000 MT
Urea : 5,94,000 MT
Methanol : 1,30,000 MT
Formic Acid : 8,000 MT Acetic Acid : 1,00,000 MT
Weak Nitric Acid : 2,47,500 MT
Conc. Nitric Acid : 66,000 MT
Calcium Amm. Nitrate : 1,42,500 MT Amm. Nitro phosphate : 1,42,500 MT
Captive Power : 50 MW
IT infrastructure : VSAT, Info tower, PKI
NCPL for Aniline and TDI
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GNFC Ammonia Plant
One of the world largest single stream Ammonia-Urea complex
Process Route : Partial oxidation of fuel oil
Ammonia Urea
Capacity 1350 MTPD 1800 MTPD
Capacity Utilization 117 % 118%
Formic acid, Acetic Acid, Aniline, TDI and Methanolplants are dependent on Ammonia plant
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Integration of Ammonia Plant with otherplants
1350 MTPD
UREA
C02
NH3
Nitro Phosphate Unit
NH3
C02
CO
Tail Gas
FORMIC ACID
SYN GAS
H2+CO2+CO
CO2
NCPL
CO
BOILER
CO
ACETIC ACIDMETHANOL 1
METHANOL 2
AMMONIAPLANT
Purge Gas.
P.G.
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Ammonia Cooling Water System
Induced draft CT : 12 no. of cells
CW circulation flow : 34,000 m3/hr
Heat Duty : 352 Mkcal/hr
CW Supply temperature: 33 Deg C.
CW Return temperature: 43 Deg C CW pump capacity : 6800 m3/hr each
CW header pressure : 3.1 barg
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Old In-house CW Treatment
In-house treatment program developedby GNFC was followed before Dec-99
SHMPOrgano-phosphate
Zinc phosphate
BiocidesCOC : 3 ~ 4
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Present Cooling Water TreatmentM/S Chembond Drewtreat treatment:
First introduced in Urea plant in 1992
Since Dec-99 in Ammonia plant
Based on:
Zinc glassy ortho -meta phosphate(KW101)
Organophosphate-PBTC with low molecularwt polymer(KW1002G)
Biocide chemicals :
Chorine Dioxide
Quaternary Ammonium compound
Dichlorophene
DBNP (Di-bromo- nitroso-phenolic comp.
Bio-dispersant (KW-BD)
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CW Treatment Monitoring
Dedicated CW water cell Monitoring of Analysis and supervision of Ammonia
CT by M/s. Chembond
Regular activities:
Daily : Performance evaluation by CW cell
Weekly: CT cells deck algae cleaning
Monthly : Sterilization of side stream filters
Review of exchangers performance
Corrosion rate monitoring
Quarterly: Review with M/s Chembond formodification in treatment; if required
Bio-fouling monitoring
Inspection and cleaning during shut down
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Benefits With better treatment and Modifying the limits
of critical parametersCOC improved to 6~6.5
Saving in CW make up : 11,000,00 m3/year.
Reduction in corrosion rate :
From 3~4 mpy to
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CW parametersMake up
waterCW
circulation
pH 7.0~8.0 6.8~7.2
Conductivity Micro mho 200~400 2500max
TH ppm 70~150 800~825
Mg Hardness ppm 25~70 250~350
Ca Hardness ppm 50~85 450~550
Chloride ppm 10~25 250max
Silica ppm 10~20 100~125
Turbidity NTU 1~2 10
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Typical CW parametersCirculating water
Ortho PO4 ppm 5~6
Poly PO4 ppm 1.5~3.0
Organo PO4 ppm 1.5~3.0
Total PO4 ppm 7~10Zinc ppm 0.5~1
TDS ppm 1500max
NH3 ppm 10TVC per ml 50,000
SRB mpn /100
ml
100
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Ammonia Synthesis Gas
Cooler E706
A case study
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History of E706
Synthesis Gas cooler- a critical
exchanger condenses 50~60% ammoniain synthesis gas loop
Original exchanger started leaking
within a year of service Frequent and severe leakages started
within a short span of time
Cause : Flow induced vibrations Replaced in July-1984 :
A better design exchanger : SS304 tubes
and split flow of CW side installed
F f N S h i G C l
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Features of New Synthesis Gas Cooler
New design exchanger installed in 1984
H.T. Area : 1445 m2
Heat Duty : 14.28 MKcal/hr
Cooling water : Shell side
In/Out temp : 33/43
No of passes : Split flow
CW flow : 1500 m3/hr
MOC : CS
Synthesis gas : Tube side
In /Out temp : 79/ 39
Pressure : 230 bar
No of pass : 2 , U-tubes
No. of tubes : 1095
MOC : SS-304
L k f E706
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Leakage of E706 After 17 years, first leakage noticed in May-2001
Process gas containing 18 % Ammonia leaks to CW side
Gas was coming out with from shell side vent
IN OUT Diff.
pH 7.4 9.1 +1.7
Ammonia 5~10 ppm 15~50 ppm +10~40Conductivity 1240 1150 -90
Ca Hardness 324 272 -52
Chloride 236 208 -32Turbidity 14 16 +4
Total Hardness 664 572 -92
ORP +320 -300 -620
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Leakage of E706Consequences
5 ~10 ppm Ammonia in CW circulationsystem
Elevated pH of CW outlet to 8.5
Chlorination limitation
High microbiological growth - nitrifyingbacteria CW supply pH tends to remain low
Biomass fouling in the exchangers
Gas pocketing in the exchangersBack pressure in the E706, less CW flowthrough it
Scaling in the exchangers of CW system
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Repair of E706 :1In October 2002 S/D
CW side back-flushed:Sludge of ammonia salts was flushed out
Tube bundle Inspected from CW I/L nozzle: Found completely blocked with white sludge
Bundle pulling out was not possible
Chemical cleaning with 5% sulphamic acidResults was not satisfactory
Shell was cut open from one side and cleaned
with high pressure JettingHydro-test at 12 barg was carried out:3 leaky tubes plugged
Leakage Persisted
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Scaling in E706
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E 706 SHELL SIDE SCALING
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Repair of E706 : 2
In Jan 03 S/D
In Jan03 opportunityChemical cleaning with 5% sulphamic acid
Leak test was taken. No leakage identified,
Why? During normal operation, press diff. between
shell and tube is very high 230 bar, cracksopen up at high pressure
Shell is low pressure part Leakage not detectable with hydro test at 12
bar pressure
R i f E706 3
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Repair of E706 : 3In April 03 S/D
A special ammonia test carried outShell plates cut and the bundle cleaned withhydro jetting
Shell pressurised to 1 bar with N2 and furtherto 2 bar with Ammonia
Leakage detected by placing Ammonia testpaper on the tube sheet and observing color
change to blue12 tubes were detected and plugged
However, CW outlet ammonia pick up and pH
still indicated leakage after start-up
o usta n perat ons
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o usta n perat onsChallenging task : To maintain the thermal
performance of E706
E706 performance deteriorated due toscaling and gas back pressure, syn gasoutlet temp increased to 50 deg C from 39deg
Load on down stream refrigeration unit wasincreased, steam consumption increasedby 4 Mt/hr
Measures Taken:
1.0 Local gas release provision
2.0 Managing Micro biological activity
3.0 Managing scaling
1 L l R l
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1. Local Gas ReleaseLocal venting
10 no. of 1 tapping were taken on-line from
the shell and connected to a 4 vent header
Shell side Safety valve was dropped & lineextended up to CT height
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VENT GAS HEADER
E706
SAFETY VALVE LINE
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2.0 Managing Micro biological activityIn presence of ammonia, it is difficult to
achieve free chlorineFor effective microbiological activitycontrol:
Dosing of Chlorine dioxide startedMore stable and effective even athigher pH value
Does not react with Ammonia andorganic comp.
Bromine based biocide was also started
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2.0 Managing Micro biological activity
Additional bio-dispersant dosing wasstarted
Frequency of Sterilization of side stream
filters increased : once a weekCW system and exchangers Monitoring bymeasuring ORP
Nitrate Nitrogen, nitrifying bacteriamonitored
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3.1 Managing Scaling
Measures taken to contain scaling:
1. Local Polymeric Dispersants dosing
Effectiveness checked by analyzingCa-Hardness at CW inlet and Outlet,
before and after dosing
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3.1 Managing Scaling
E706 IN E706 OUT Diff
pH 6.8 8.5 +1.7
Ca H 450 440 -10
TIP 6.7 5.4 - 1.3
Before dosing dispersants
After dosing dispersantsE706 IN E706 OUT Diff
pH 6.8 8.9 +2.1
Ca H 452 448 - 4
TIP 10.3 10.6 +0.3
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3.2 Managing Scaling2. Back flushing:
Loose scale partially removed by theexchanger back flushing during shortinterruptions
3. Nitrogen Bumping:
Twice in a day Low pressure N2blowing for half an hour was done inthe exchanger for removing loose scale
The removal of scale is ensured byanalyzing CW outlet sample indicatingrise in Turbidity by 50 ~90 NTU and risein Ca-Hardness by 10 ~25 ppm.
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Effect of Nitrogen Bumping
E706 Ca-Hardn
ess
Rise in Ca-Hardness
Turbidity Rise inTurbidity
CW Inlet 464 -- 18 --
CW OutletBeforeBumping
460 - 4 28 +10
CW outletAfter
Bumping
480 +20 95 +77
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3.3 Managing Scaling
4. Local CW make up at E706 inlet
To reduce Hardness- a key factor forscaling
CW outlet hardness was reduced from700 ppm to 550 ppm
5. Local Sulphamic acid dosing To reduce local pH
Special arrangement made for dosing
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SULPHAMIC ACIDDOSING TANK
LOCAL WATER MAKE-UP
E706
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Plant Operation could besustained for 3 years till the
replacement of theexchanger in April 2004
with the effective problemspecific treatment
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Conclusion The problems related to cooling water systems
can lead to heavy production and energy loss.This can be effectively handled without affectingproduction and continuity of the plant by thoroughunderstanding of the process as well as CW
chemistry involved. Cooling water treatment is a specialized subject.
A lot of research and improvements are takingplace in this field. This knowledge is available to
industry through experts in the field.
Industry should adopt the relevant features ofadvancements for improvement in the system.
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THANK YOU