Ammonia CW Case Study 08 Feb 06

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    Cooling Water Treatment

    -An Experience at GNFC

    By N. B. Bhatt and A.M. Vashi

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    GNFC AT A GLANCE

    Incorporation : May10,1976

    Capacity Per Annum Ammonia : 4,45,000 MT

    Urea : 5,94,000 MT

    Methanol : 1,30,000 MT

    Formic Acid : 8,000 MT Acetic Acid : 1,00,000 MT

    Weak Nitric Acid : 2,47,500 MT

    Conc. Nitric Acid : 66,000 MT

    Calcium Amm. Nitrate : 1,42,500 MT Amm. Nitro phosphate : 1,42,500 MT

    Captive Power : 50 MW

    IT infrastructure : VSAT, Info tower, PKI

    NCPL for Aniline and TDI

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    GNFC Ammonia Plant

    One of the world largest single stream Ammonia-Urea complex

    Process Route : Partial oxidation of fuel oil

    Ammonia Urea

    Capacity 1350 MTPD 1800 MTPD

    Capacity Utilization 117 % 118%

    Formic acid, Acetic Acid, Aniline, TDI and Methanolplants are dependent on Ammonia plant

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    Integration of Ammonia Plant with otherplants

    1350 MTPD

    UREA

    C02

    NH3

    Nitro Phosphate Unit

    NH3

    C02

    CO

    Tail Gas

    FORMIC ACID

    SYN GAS

    H2+CO2+CO

    CO2

    NCPL

    CO

    BOILER

    CO

    ACETIC ACIDMETHANOL 1

    METHANOL 2

    AMMONIAPLANT

    Purge Gas.

    P.G.

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    Ammonia Cooling Water System

    Induced draft CT : 12 no. of cells

    CW circulation flow : 34,000 m3/hr

    Heat Duty : 352 Mkcal/hr

    CW Supply temperature: 33 Deg C.

    CW Return temperature: 43 Deg C CW pump capacity : 6800 m3/hr each

    CW header pressure : 3.1 barg

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    Old In-house CW Treatment

    In-house treatment program developedby GNFC was followed before Dec-99

    SHMPOrgano-phosphate

    Zinc phosphate

    BiocidesCOC : 3 ~ 4

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    Present Cooling Water TreatmentM/S Chembond Drewtreat treatment:

    First introduced in Urea plant in 1992

    Since Dec-99 in Ammonia plant

    Based on:

    Zinc glassy ortho -meta phosphate(KW101)

    Organophosphate-PBTC with low molecularwt polymer(KW1002G)

    Biocide chemicals :

    Chorine Dioxide

    Quaternary Ammonium compound

    Dichlorophene

    DBNP (Di-bromo- nitroso-phenolic comp.

    Bio-dispersant (KW-BD)

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    CW Treatment Monitoring

    Dedicated CW water cell Monitoring of Analysis and supervision of Ammonia

    CT by M/s. Chembond

    Regular activities:

    Daily : Performance evaluation by CW cell

    Weekly: CT cells deck algae cleaning

    Monthly : Sterilization of side stream filters

    Review of exchangers performance

    Corrosion rate monitoring

    Quarterly: Review with M/s Chembond formodification in treatment; if required

    Bio-fouling monitoring

    Inspection and cleaning during shut down

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    Benefits With better treatment and Modifying the limits

    of critical parametersCOC improved to 6~6.5

    Saving in CW make up : 11,000,00 m3/year.

    Reduction in corrosion rate :

    From 3~4 mpy to

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    CW parametersMake up

    waterCW

    circulation

    pH 7.0~8.0 6.8~7.2

    Conductivity Micro mho 200~400 2500max

    TH ppm 70~150 800~825

    Mg Hardness ppm 25~70 250~350

    Ca Hardness ppm 50~85 450~550

    Chloride ppm 10~25 250max

    Silica ppm 10~20 100~125

    Turbidity NTU 1~2 10

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    Typical CW parametersCirculating water

    Ortho PO4 ppm 5~6

    Poly PO4 ppm 1.5~3.0

    Organo PO4 ppm 1.5~3.0

    Total PO4 ppm 7~10Zinc ppm 0.5~1

    TDS ppm 1500max

    NH3 ppm 10TVC per ml 50,000

    SRB mpn /100

    ml

    100

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    Ammonia Synthesis Gas

    Cooler E706

    A case study

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    History of E706

    Synthesis Gas cooler- a critical

    exchanger condenses 50~60% ammoniain synthesis gas loop

    Original exchanger started leaking

    within a year of service Frequent and severe leakages started

    within a short span of time

    Cause : Flow induced vibrations Replaced in July-1984 :

    A better design exchanger : SS304 tubes

    and split flow of CW side installed

    F f N S h i G C l

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    Features of New Synthesis Gas Cooler

    New design exchanger installed in 1984

    H.T. Area : 1445 m2

    Heat Duty : 14.28 MKcal/hr

    Cooling water : Shell side

    In/Out temp : 33/43

    No of passes : Split flow

    CW flow : 1500 m3/hr

    MOC : CS

    Synthesis gas : Tube side

    In /Out temp : 79/ 39

    Pressure : 230 bar

    No of pass : 2 , U-tubes

    No. of tubes : 1095

    MOC : SS-304

    L k f E706

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    Leakage of E706 After 17 years, first leakage noticed in May-2001

    Process gas containing 18 % Ammonia leaks to CW side

    Gas was coming out with from shell side vent

    IN OUT Diff.

    pH 7.4 9.1 +1.7

    Ammonia 5~10 ppm 15~50 ppm +10~40Conductivity 1240 1150 -90

    Ca Hardness 324 272 -52

    Chloride 236 208 -32Turbidity 14 16 +4

    Total Hardness 664 572 -92

    ORP +320 -300 -620

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    Leakage of E706Consequences

    5 ~10 ppm Ammonia in CW circulationsystem

    Elevated pH of CW outlet to 8.5

    Chlorination limitation

    High microbiological growth - nitrifyingbacteria CW supply pH tends to remain low

    Biomass fouling in the exchangers

    Gas pocketing in the exchangersBack pressure in the E706, less CW flowthrough it

    Scaling in the exchangers of CW system

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    Repair of E706 :1In October 2002 S/D

    CW side back-flushed:Sludge of ammonia salts was flushed out

    Tube bundle Inspected from CW I/L nozzle: Found completely blocked with white sludge

    Bundle pulling out was not possible

    Chemical cleaning with 5% sulphamic acidResults was not satisfactory

    Shell was cut open from one side and cleaned

    with high pressure JettingHydro-test at 12 barg was carried out:3 leaky tubes plugged

    Leakage Persisted

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    Scaling in E706

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    E 706 SHELL SIDE SCALING

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    Repair of E706 : 2

    In Jan 03 S/D

    In Jan03 opportunityChemical cleaning with 5% sulphamic acid

    Leak test was taken. No leakage identified,

    Why? During normal operation, press diff. between

    shell and tube is very high 230 bar, cracksopen up at high pressure

    Shell is low pressure part Leakage not detectable with hydro test at 12

    bar pressure

    R i f E706 3

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    Repair of E706 : 3In April 03 S/D

    A special ammonia test carried outShell plates cut and the bundle cleaned withhydro jetting

    Shell pressurised to 1 bar with N2 and furtherto 2 bar with Ammonia

    Leakage detected by placing Ammonia testpaper on the tube sheet and observing color

    change to blue12 tubes were detected and plugged

    However, CW outlet ammonia pick up and pH

    still indicated leakage after start-up

    o usta n perat ons

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    o usta n perat onsChallenging task : To maintain the thermal

    performance of E706

    E706 performance deteriorated due toscaling and gas back pressure, syn gasoutlet temp increased to 50 deg C from 39deg

    Load on down stream refrigeration unit wasincreased, steam consumption increasedby 4 Mt/hr

    Measures Taken:

    1.0 Local gas release provision

    2.0 Managing Micro biological activity

    3.0 Managing scaling

    1 L l R l

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    1. Local Gas ReleaseLocal venting

    10 no. of 1 tapping were taken on-line from

    the shell and connected to a 4 vent header

    Shell side Safety valve was dropped & lineextended up to CT height

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    VENT GAS HEADER

    E706

    SAFETY VALVE LINE

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    2.0 Managing Micro biological activityIn presence of ammonia, it is difficult to

    achieve free chlorineFor effective microbiological activitycontrol:

    Dosing of Chlorine dioxide startedMore stable and effective even athigher pH value

    Does not react with Ammonia andorganic comp.

    Bromine based biocide was also started

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    2.0 Managing Micro biological activity

    Additional bio-dispersant dosing wasstarted

    Frequency of Sterilization of side stream

    filters increased : once a weekCW system and exchangers Monitoring bymeasuring ORP

    Nitrate Nitrogen, nitrifying bacteriamonitored

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    3.1 Managing Scaling

    Measures taken to contain scaling:

    1. Local Polymeric Dispersants dosing

    Effectiveness checked by analyzingCa-Hardness at CW inlet and Outlet,

    before and after dosing

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    3.1 Managing Scaling

    E706 IN E706 OUT Diff

    pH 6.8 8.5 +1.7

    Ca H 450 440 -10

    TIP 6.7 5.4 - 1.3

    Before dosing dispersants

    After dosing dispersantsE706 IN E706 OUT Diff

    pH 6.8 8.9 +2.1

    Ca H 452 448 - 4

    TIP 10.3 10.6 +0.3

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    3.2 Managing Scaling2. Back flushing:

    Loose scale partially removed by theexchanger back flushing during shortinterruptions

    3. Nitrogen Bumping:

    Twice in a day Low pressure N2blowing for half an hour was done inthe exchanger for removing loose scale

    The removal of scale is ensured byanalyzing CW outlet sample indicatingrise in Turbidity by 50 ~90 NTU and risein Ca-Hardness by 10 ~25 ppm.

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    Effect of Nitrogen Bumping

    E706 Ca-Hardn

    ess

    Rise in Ca-Hardness

    Turbidity Rise inTurbidity

    CW Inlet 464 -- 18 --

    CW OutletBeforeBumping

    460 - 4 28 +10

    CW outletAfter

    Bumping

    480 +20 95 +77

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    3.3 Managing Scaling

    4. Local CW make up at E706 inlet

    To reduce Hardness- a key factor forscaling

    CW outlet hardness was reduced from700 ppm to 550 ppm

    5. Local Sulphamic acid dosing To reduce local pH

    Special arrangement made for dosing

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    SULPHAMIC ACIDDOSING TANK

    LOCAL WATER MAKE-UP

    E706

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    Plant Operation could besustained for 3 years till the

    replacement of theexchanger in April 2004

    with the effective problemspecific treatment

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    Conclusion The problems related to cooling water systems

    can lead to heavy production and energy loss.This can be effectively handled without affectingproduction and continuity of the plant by thoroughunderstanding of the process as well as CW

    chemistry involved. Cooling water treatment is a specialized subject.

    A lot of research and improvements are takingplace in this field. This knowledge is available to

    industry through experts in the field.

    Industry should adopt the relevant features ofadvancements for improvement in the system.

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    THANK YOU