TRUNION GATE RESISTANCE ANALYSIS - … 3 MOTIVATION FOR WORK •Folsum Tainter Gate Failure •FERC...

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TRUNION GATE RESISTANCE ANALYSIS

Applied on Diablo Dam, Diablo WA

Robert Gordon| May 7, 2015

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DIABLO DAM GENERAL INFO

• Built: 1927-1929

• Concrete Arch Dam With Gravity Abutments

o389 feet high

o1180 feet at crest

o19 Tainter Radial Gate 20’-6” wide, 18’ to max. Lake

oGates 1-3 Automated in ~1980

oGates 4-19 Operated by Portable Hoist

oNormal Usage Sequence is 2, 3, Teens

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MOTIVATION FOR WORK

• Folsum Tainter Gate Failure

• FERC Part 12 Inspection Item

oModel and Determine Maximum Acceptable

Friction

oFriction Test Gates and Determine Current

Condition

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PRELIMINARY TESTING

• Contracted Consultant For:

oFEA Model of Gate

oDetermine Method to Test

oTest and Determine Friction Factor on a Portion of

the Gates

• SCL Assisted with Initial Testing

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METHOD OF TEST TO DETERMINE TRUNNION

FRICTION

• Cantilevered Beam (73” long) Temporarily

Mounted at Each Trunnion

• Digital Dial Indicator Mounted at The End Beam

• Serial Connection Between Indicator and PC

• Data Collected Using PC Running LabVIEW

• Collect Continuous Data at 10 Hz

• Raise Gate 1 Foot and 2 Foot

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FRICTION TEST RESULTS

• Gate 2 Friction

o0.9 Right

o0.6 Left

•Maximum

Acceptable

Friction Factor

0.3: this is

about

0.56mm*2

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ACCESS TO LOCATION

• Constructed Work

Platform

• Install Gate Restraint

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REMOVAL OF TRUNNION BUSHING CARRIER

• Remove Lead Paint on Trunnion

• Remove 18 1” Rivets Per Side

• Remove Bushing Carrier

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TRUNNION PINS

• Trunnion Surface Corroded ~0.025” deep

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•Machined With Climax PL2000 Portable Lathe

oRemoved ~0.050” off Diameter

oPolished to ~10 Ra

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IMPROVEMENTS TO BUSHING

•Original Bushing had 1 Port with “X” Grove

~+/- 30 Degree of Coverage

•New Bushing (Improve Grease Distribution)

oOuter Circumferential Groove

o4 ports OD to ID

o4 Distribution Bars

o2 Circumferential Grease Dams

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BUSHING CARRIER WORK

• Bore Was Damaged From Bushing Movement

•Medium Porosity Casting

• Counter Bore Bolt Holes

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REASSEMBLY OF TRUNNION

• Bolted Both Sides Together

oSocket Head Cap Screws

oNordlock Lock Washers

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FINAL TESTING

• Dry Gate Opening Test With Beam/Indicator

• Conduct Full Gate Opening

•Wet Gate Opening Test With Beam/Indicator

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TRANSDUCER, LOCATIONS, AND FIXTURES

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SIMPLIFIED LABVIEW DAQ CODE

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ACCESS TO INSTRUMENTED LOCATION

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PRE RING TEST

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WET GATE FRICTION TESTING DATA

• Repaired Trunnion Friction ~0.07

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ALTERNATIVE METHODS TO MEASURE FRICTION

•Mount Strain Gages on Involved Elements

• Strain Gage on Transferable Beam

• Laser/Camera/Burn Paper

• Encoders on Gate Hub

• Load Cells on Hoist Cable/Actuator

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KEY FEATURES IN TESTING SYSTEM

•Need Real-time Indications During Testing

•Method to Archive Test Data

• High Resolution

• Rigid Test Fixtures/High Natural Frequencies

•Weatherproof & Robust

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FUTURE WORK

• Refurbish of All 19 Gates To Greaseless Design

oReduced Future Labor Costs From Greasing

oBronze Bushing Cost ~= to Greaseless Bushing Cost

oLess Environmental Waste

o Instigation Cost Same

o Improved Worker Safety

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NEW GREASELESS BUSHING/TRUNNION DESIGN

• Turn Existing Trunnion to Round and Smooth

• Thermally Shrink Fit Stainless Steel Sleeve to

Trunnion Shaft

• Bore Out Cast Bushing Carrier for New Greaseless

Bushing

• Add Two Energized O-ring Seals on

Trunnion/Bushing Ends

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