Post on 09-Dec-2021
I
DC-DC 4-Switch Buck-Boost Converter for Energy Harvesting from Elliptical Machines
by
Alexander Samietz
Gustavo Guzman
Senior Project
Electrical Engineering Department
California Polytechnic State University
San Luis Obispo
2018
II
TABLE OF CONTENTS
Section Page
Abstract………………………………………………………………………………………. 1
Chapter 1: Introduction………………………………………………………………………. 2
Chapter 2: Customer Needs, Requirements, and Specifications…………………………….. 3
1. Customer Needs Assessment………………………………………………………… 3
2. Requirements and Specifications……………………………………………………. 3
Chapter 3: Functional Decomposition………………………………………………………. 6
Chapter 4: Project Planning…………………………………………………………………. 8
Chapter 5: Circuit Design and Simulations…………………………………………………. 11
Chapter 6: Component Selection and PCB Layout…………………………………………. 26
Chapter 7: Assembly………………………………………………………………………… 41
Chapter 8: Testing…………………………………………………………………………… 42
Chapter 9: Future Plans and Takeaways…………………………………………………….. 43
Bibliography…….…………………………………………………………………………… 44
Appendices
A. Senior Project Analysis…………………………………………………………………... 47
B. LTSpice .net File ………………………………………………………………………… 51
III
Lists of Tables and Figures
TABLES Page
Table I. DC-DC Buck-boost Converter Requirements & Specifications……………………… 4
Table II. DC-DC Buck-boost Converter Project Deliverables………………………………… 5
Table III. Level 0 DC-DC Buck-boost converter Functional Requirement…………………… 6
Table IV. Level 1 DC-DC Buck-boost converter Functional Requirement…………………… 7
Table V. DC-DC Buck-boost converter Cost Estimates………………………………………. 9
Table VI. Summary of Actual Project Costs………………………………………………….. 10
Table VII. Maximum ratings for MOSFETs BSZ100N06lS3G……………………………… 13
Table VIII. Maximum Voltage Ratings for the Four External Switches Based on Simulation 14
Table IX. BSZ100N06LS3G NMOS Specifications…………………………………………. 26
FIGURES
Figure I. Level 0 DC-DC Buck-boost Converter Block Diagram…....……………………….. 6
Figure II. Level 1 DC-DC Buck-boost Converter Block Diagram…....………………………. 6
Figure III. EE 460, EE 461, and EE 462 Gantt Charts………………………………………… 8
Figure IV. LT8390 Test Fixture Schematic…………………………………………………… 11
Figure V. Safe Operating Area of the N-channel MOSFET BSZ100N06LS3G……………… 14
Figure VI. 36 V output voltage, < 1 V output voltage ripple with 0.277 Electronic load…….. 16
Figure VII. Boost region inductor current waveform using electronic load…………………... 16
Figure VIII. VDS waveforms for four external MOSFET switches using electronic load…….. 17
Figure IX. 36 V output voltage, <1 V output voltage ripple with 130 Ω resistive load………. 17
Figure X. Boost region inductor current waveform using a resistive load……………………. 18
Figure XI. VDS waveforms for four external MOSFET switches using a resistive load……… 18
Figure XII. 36 V output voltage, <1 V output voltage ripple with 5.4 An electronic load…… 19
Figure XIII. Buck region inductor current waveform using electronic load………………….. 19
Figure XIV. VDS waveforms for the four external MOSFET switches using electronic load… 20
Figure XV. 35.61 V output voltage, <1 V output voltage ripple with 5.3 Ω resistive load…… 20
Figure XVI. Buck region inductor current waveform using a resistive load………………….. 21
Figure XVII. VDS waveforms for the four external MOSFET switches using a resistive load... 21
IV
Figure XVIII. 36.19 V output voltage, <1 V output voltage ripple with 3.7 An electronic load 22
Figure XIX. Buck-boost region inductor current waveform using an electronic load……… 23
Figure XX. VDS waveforms for the four external MOSFET switches using an electronic load 23
Figure XXI. 36.19 V output voltage, <1 V output voltage ripple with 10 Ω resistive load…. 24
Figure XXII. Buck-boost region inductor current waveform using a resistive load………… 24
Figure XXIII: VDS waveforms for the four external MOSFET switches using a resistive load 25
Figure XXIV. Schematic for First Revision of Board………………………………………. 27
Figure XXV. Front Layer for First Revision of Board………………………………………. 28
Figure XXVI. Back Layer for First Revision of Board……………………………………… 29
Figure XXVII. Schematic for Second Revision of Board…………………………………… 31
Figure XXVIII. Front Layer for Second Revision of Board………………………………… 32
Figure XXIV. Back Layer for Second Revision of Board…………………………………... 33
Figure XXX. Front Layer for Third Revision of Board……………………………………... 34
Figure XXXI. Back Layer for Third Revision of Board…………………………………….. 35
Figure XXXII. Schematic for Final Revision of Board……………………………………... 37
Figure XXXIII. Front Layer for Final Revision of Board…………………………………… 38
Figure XXXIV. Back Layer for Final Revision of Board…………………………………… 39
Figure XXXVI. Final soldered PCB………………………………………………………… 41
1
Abstract
The senior project report documents the process of replacing the network of resistors inside an elliptical
machine with a DC-DC buck-boost converter. The buck-boost DC-DC converter accepts a wide input range of
5-60 Volts, with an output of 36 Volts for the most efficient use of the already available microinverter. The
microinverter reclaims the lost energy and safely distributes it back to the electrical grid. The addition of this project
reduces heat emissions from wasted energy and shrinks the carbon footprint of its users.
2
Chapter 1: Introduction
This project intends to provide a solution to the wasted, unused energy produced by the Precor elliptical
workout machine. The Cal Poly recreation center currently houses dozens of Precor elliptical machines all capable
of harnessing lost energy. The opportunity for an entity to develop a process that harnesses the energy relates ideally
to the Energy Harvesting from Exercise Machines project at Cal Poly. The project focuses on the DC-DC converter.
The DC-DC converter stabilizes the sporadic and unpredictable elliptical output and converts the output to a desired
input voltage for the microinverter. The project undergoes the design, testing, and revision process of the DC-DC
converter that achieves maximum efficiency.
Professor Braun first conceived this idea in 2007 and has produced multiple projects since its inception [1].
This report takes advantage of a relatively new buck/boost controller developed by Linear Technology. The
controller has a large input range of 4-60 Volts, precisely the voltage range produced by an elliptical machine.
Efficiency of the controller exceeds 90% for its complete input range, allowing for minimal energy loss. [2-4]. A
pre-purchased microinverter reduces project complications. This report references work done by a previous student
at Cal Poly, Angelo Gallardo, who used the same controller in his master’s thesis [5] and Andrew Forster who
developed a four-switch buck-boost DC-DC converter [5,6].
Currently, several companies provide solutions to the problem mentioned above. For example, The Green
Revolution and ReSource Fitness manufacture entirely new devices including an internal energy harvester [7].
ReRev retrofits old exercise machines that harness the energy. ReRev has outfitted old machines at over 28
universities across the U.S. [8]. The high demand for energy harvesting machines creates an abundant opportunity
for development. However, an investment return for consumers takes a long time before benefits show. By
producing a more efficient, cost friendly solution, not only do investors earn their money back quicker, but the
environment sees a positive, sustainable impact.
The elliptical machines work by submitting the user to physical resistance using a magnetic synchronous
generator. The more resistance, the more current the magnetic generator produces, thus creating a harder workout
for the user [9]. The rectified AC voltage, through a network of resistors dissipates as heat. Intervening in this
process and replacing the network of resistors with a DC-DC generator mentioned above, creates an opportunity to
harness wasted energy.
Cal Poly’s attempt at harnessing unused energy in previous years had minimal success. This included
purchasing off-the-shelf DC-DC converters and interfacing with the elliptical machines. The efficiency of the
converters topped off at about 40%, but at higher power levels the converter failed [4]. As a result, the project
necessitates making the converter more efficient than previous attempts. This report documents the design process
and provides the results. To determine what to design, the customer’s needs, requirements, and specifications were
investigated.
3
Chapter 2: Customer Needs, Requirements, and Specifications
This chapter highlights the customer needs and marketing requirements important to the design process of the
system.
Customer Needs
The intended customers for this product consist of gym owners or those who have a personal gym. To elicit
the customer needs, interviews were conducted with those who consider themselves environmentalists. This
included gym regulars and an environmental engineer. When purchasing the product, the customer reiterated the
goal of sustainability thinking. The product’s major appeal to consumers is the system’s ability to harvest wasted
energy from a machine and turn it into usable, reliable energy. Any process that makes the product more effective,
the more the consumer wants it. A customer need that overshadows the project stems from project price. A customer
would refuse to purchase the product, if the system does not guarantee an investment return, meaning the product
pays itself off before the end of the products lifecycle. Minimizing the system’s power needs would guarantee the
consumer’s investment is returned. Designing the product that allowed consumer installation within the elliptical
machine reduces cost. Requiring the device to fit inside the elliptical machine would remove extra casing needed.
Easy installation would save the customer money by avoiding a professional for proper installation. The most
important need, especially to the Recreation Center, is safety. The Recreation Center has strict guidelines regarding
safety due to the vast number of users it sees every day. No matter the performance of the machine, if it is not safe it
will not be purchased. The design process will emphasize this.
Marketing Requirements and Specifications
The requirements and specifications change based on customer needs, and technical and performance
constraints. Adding unnecessary costs to the product would reduce its viability for potential customers. For example,
adding extra casing or having extra installation steps would scare customers away, potentially to a competitor’s
product that avoids unnecessary costs and extra installation steps. Cost is also an important system consideration.
The product should pay itself back before the end of its lifecycle, so having a cost higher than the savings produced
by the product would make it unviable. Designing the product to work on different exercise machines would not
only produce more energy for the consumer, but also would expand the customer-base. Lastly, the product’s
overarching theme focuses on efficiency. The product should achieve higher efficiency than previous related
projects [6]. If the system consumes more power than it produces, then it defeats the purpose of the project.
4
Table I below shows marketing requirements, engineering specifications, and justifications.
TABLE I
DC-DC BUCK-BOOST CONVERTER REQUIREMENTS AND SPECIFICATIONS
Marketing
Requirements
Engineering
Specifications Justification
4,5 Output 36 Volts within ±1.8 Volts of the
desired value and output a current no more
than 8 Amps.
36 Volts achieves highest efficiency for the
purchased microinverter [5]. Allowing for the
highest efficiency reduces product waste.
5 Operates with a DC-DC controller
efficiency of 90% or greater over the input
voltage range.
To recoup production costs, the project requires
high efficiency, which allows the user to
maximize money savings.
4,5
Accepts a voltage range of 5-60 Volts and
accept an input current no more than 4
Amps.
Depending on the user and intensity of the
workout, the voltage produced varies. The
micro inverter takes a max input current of
7 A [4].
1
The system must meet all UL 1741 and
IEEE 1547 requirements.
These requirements protect the grid, keep the
system safe, reliable and environmentally
responsible.
1,2
Fits within a 7”x7”x4” rectangular volume,
weigh less than 1 kg, and fit inside the
elliptical
Should not have to add extra casing which
would add unnecessary cost to the system.
Having the controller and converter outside of
the machine could cause congested areas
around it.
3
Production cost less than $360.
Production cost comes from conservative
estimate of 100W workout, with 90% inverter
efficiency, DC-DC converter efficiency of
80%, and 12 hours of machine use per day for
41 weeks out of a year [10]. If the system
doesn’t generate money, or break even, over
the product lifetime’s course, then no monetary
reason to use it.
3,5
Connectors should use spade lugs
to connect to the elliptical machine and
banana
plugs to connect to the DCDC
converter [4].
Familiar connectors allow for quick and easy
installation [5].
Marketing Requirements
1. Safety
5
2. Small and compact
3. Low-cost
4. Versatile
5. Efficient
Table II below shows the deliverables and their corresponding due dates. The next chapter deals with the functional
decomposition of the system.
TABLE II
DC-DC BUCK-BOOST CONVERTER DELIVERABLES
Delivery Date Deliverable Description
April 16th Design Review
June 14th EE 461 report
June 14th First Version of Board Layout
December 6th EE 462 demo
ABET Sr. Project Analysis
Sr. Project Expo Poster
December 15th EE 462 Report
Chapter 3 goes into detail about the high level and low level functional decompositions. This structure allows an
easy-to-follow process of how the system works.
6
Chapter 3: Functional Decomposition
To have a grasp in the macro and micro levels to which this system is being designed, multiple block diagrams are
created to map out different levels of the design.
Figure 1 shows the level 0 block diagram for the system.
Figure I: Level 0 Energy DC-DC Buck-Boost Converter Block Diagram.
Table III shows level 0 system functional requirements. The user pedals an existing elliptical machine at different
speeds, producing a range of voltages. The system converts the voltage range into usable energy that’s delivered to
the grid at 120 Vac, 15A and 60 Hz.
TABLE III:
DC-DC BUCK-BOOST CONVERTER FUNCTIONAL REQUIREMENTS
Module System
Input Gym user pedaling elliptical machine at variable speeds producing 5-60 Vdc
Output Regulated 36 Vdc
Function The user utilizing the elliptical machine produces voltages of 5-60 volts. A device captures the
energy and converts it to an acceptable 36 volts for the micro inverter, which delivers it safely to
the grid.
In Figure II, the level 1 block diagram shows the basic inputs and outputs for the EHFEM project. The level
1 architecture contains the elliptical machine operated by a user, DC-DC converter, micro inverter, and the electrical
grid. The elliptical machine produces 5-60 Vdc that feeds into the DC-DC Converter, which steps down or up the
input voltage to a constant 36 Vdc output voltage. The micro inverter takes the 36 Vdc output voltage and inverts it
to 120Vac at 60 Hz.
.
Figure II: Level 1 EHFEM Block Diagram
Table IV shows level 1 functional requirements, which contain all subsystems. Each module has inputs,
corresponding outputs, and main functions. The level 1 architecture consists of the user, elliptical machine, DC-DC
converter, micro inverter, and the electrical grid.
5-60 Volts DC 36 Volts DC
7
TABLE IV:
DC-DC BUCK-BOOST CONVERTER FUNCTIONAL REQUIREMENTS
Module Elliptical Machine DC-DC Converter Micro inverter Electrical Grid
Input User DC Voltage range
5-60 V
Constant 36 Vdc
below 7A
120 Vac at 15 A and
60 Hz
Output DC Voltage range
5-60 V
Constant 36 Vdc
below 7 A
120 Vac 60 Hz at
15 A
Usable Energy
Functionality Converts physical
movement into DC
voltages
Steps up/down the
input voltage into
constant output
voltage
Converts output
voltage into 120 Vac
at 15 A and 60 Hz
Delivers power
Chapter 4 goes into detail about the projects schedule, laying out a plan for deadlines to be met. Working out the
projects schedule provides a timeline for the delivery of necessary components.
8
Chapter 4: Project Planning
This chapter highlights the timing and costs of the project and its planning. Figure 3 shows the timeline project using
a Gantt chart. The project timeline separates into three senior project classes which allow two designs, build, and test
iterations with the final iteration due week eight of fall quarter. 461 and 462 include assigned individual tasks. The
final figure represents the actual timeline which transpired to date.
Figure IIIa: EE 460 Gantt Chart
Figure IIIb: EE 461 Gantt Chart
Figure IIIb: EE 462 Gantt Chart
Figure IIId: EE 461 Actual Gantt Chart
9
Figure IIIe: EE 462 Actual Gantt Chart
The cost of the project can be estimated using three different measures of cost: most optimistic, most likely, and
most pessimistic. These are averaged to find the most likely cost. This was done with time duration to find the most
likely amount of hours to complete the project.
𝐶𝑜𝑠𝑡 =𝑐𝑜𝑠𝑡𝑚𝑜𝑠𝑡 𝑜𝑝𝑡𝑖𝑚𝑖𝑠𝑡𝑖𝑐+4𝑐𝑜𝑠𝑡𝑚𝑜𝑠𝑡 𝑙𝑖𝑘𝑒𝑙𝑦+𝑐𝑜𝑠𝑡𝑚𝑜𝑠𝑡 𝑝𝑒𝑠𝑠𝑖𝑚𝑖𝑠𝑡𝑖𝑐
6=
20,000+92,000+26,000
6= $23,000 (1)
𝐸𝑥𝑝𝑒𝑐𝑡𝑒𝑑 𝑇𝑖𝑚𝑒 =𝑇𝑜+4𝑇𝑚+𝑇𝑝
6=
100+600+200
6= 150 ℎ𝑜𝑢𝑟𝑠 (2)
TABLE V
SUMMARY OF PROJECT COSTS
Item Cost Comments
Labor
$23,000
According to Andrew Forster’s previous work, using 420
hours of project time and an hourly rate of $56.25
determines labor costs [6]. The labor costs using the
PERT analyis closely relates to Forster’s labor costs.
Anticipated Parts
$39.71
According to Andrew Forster, final bill of material for
components resulted in $39.71 for one PCB board [6].
However, anticipated parts cost could change.
PCB Fabrication
$92.39
Andrew Forster’s previous thesis work calculates PCB
Fabrication cost to $92.39 [6]. However, PCB fabrication
could change.
Applying the PERT analysis provides a rough estimate of project duration and labor costs. For labor costs, if
assumed $20,000 for most optimistic, $23,000 for most likely, and $26,000 for most pessimistic, then according to
equation 1, labor costs estimate at $23,000. For project duration, if assumed 100 hours as most optimistic, 150 hours
for most likely, and 200 hours for most pessimistic, then according to equation 2, project duration estimates at 150
hours. The actual costs incurred were more than anticipated. These are documented below in Table VI:
10
TABLE VI
SUMMARY OF ACTUAL PROJECT COSTS
Item Cost Comments
Labor
$23,000
Using 420 hours of project time and an hourly rate of
$56.25 determines labor costs [6]. The labor costs using
the PERT analysis closely relates to Forster’s labor costs.
Parts
$306.6
Buying three of each component increased the total
amount of parts spent on the project
PCB Fabrication
$62.65
Buying three PCB’s to allow for errors in assembly
increased the cost.
The following chapter details the circuit design and simulation process and the challenges encountered. Each
iteration shows problems seen and how the situation was remedied.
11
Chapter 5: Circuit Design and Simulations
This chapter goes through the circuit design and simulation phase of the project. Simulation through SPICE is the
preferred choice for testing circuit designs. The advantages to simulation prototyping is the rapid results of the
testing and the very low cost associated with it. The circuit design is built around the LT8390, Linear Technologies
60V Synchronous 4-Switch Buck-Boost Controller, and as a starting point, the test fixture schematic pre-built in the
software was used. The .net file used for the simulation can be found in appendix B.
Figure IV: LT8390 test fixture schematic.
The following specifications were laid out and used to guide the design:
1. 𝑉𝑖𝑛 ∈ [5,60] V
2. 𝑉𝑜𝑢𝑡 = 36 V 3. 𝐼𝑜𝑢𝑡𝑚𝑎𝑥 = 7 A
4. ∆𝑉𝑜𝑢𝑡 = 1 V
5. 𝜂 >= 90%
These goals were derived from the specifications Table I. These specifications, however, were uncertain and shifted
upon further iterations. To avoid having to fully simulate multiple inputs, the following corner cases were used:
1. 𝑉𝑖𝑛 = 10 𝑉: 𝐵𝑜𝑜𝑠𝑡 𝑀𝑜𝑑𝑒
2. 𝑉𝑖𝑛 = 60 𝑉: 𝐵𝑢𝑐𝑘 𝑀𝑜𝑑𝑒
3. 𝑉𝑖𝑛 = 37 𝑉: 𝐵𝑢𝑐𝑘 𝐵𝑜𝑜𝑠𝑡 𝑀𝑜𝑑𝑒
Using these four test cases, it was assumed that the cases in the middle will follow the same success as the corner
cases. Both these test cases were done with two separate loads. One fully resistive load, and the other an electronic
load. The starting point for the simulations were provided from Linear Technology’s test fixture circuit for the
LT8390. Modifications were made to meet our specifications above.
The first goal was to modify the circuit to produce a 36 V output. This was done by altering the feedback resistor
network by using equation 1 provided by the datasheet [2]
12
𝑉𝑂𝑈𝑇 = 1𝑉 ×𝑅3+𝑅4
𝑅4 [2] (3)
The LT8390 has a voltage feedback pin FB that can be used to program a constant-voltage output, by selecting
appropriate values for R3 and R4. In our case, R3 was set to 84.5kΩ, and R4 to 2.4kΩ. Ensuring that the total
resistance of the network is large minimizes current flow through the divider network, hence improving efficiency.
Selected values are based upon actual resistor values in the market. 0.5% standard resistor values were selected to
reduce noise and improve output voltage accuracy.
The switching frequency of the LT8390 is set by an internal oscillator, using a constant frequency control scheme
between 150 kHz and 650 kHz Selection of switching frequency affects efficiency and component size. Low
frequency operation improves efficiency by reducing MOSFET switching losses. Since the projects application
emphasizes high efficiency and not component sizing, the lowest switching frequency was selected. The switching
frequency is set by connecting an appropriate resistor from pin RT to ground. A resistor value of 309 k8Ω which
corresponds to 150 kHz was used
The switching frequency and inductor selection are interrelated in that higher switching frequencies allow the use of
smaller inductor and capacitor values. Using equation 2 and 3 from the datasheet, the inductor value was properly
chosen:
𝐿𝑏𝑢𝑐𝑘 >𝑉𝑜𝑢𝑡∗(𝑉𝑖𝑛𝑚𝑎𝑥−𝑉𝑜𝑢𝑡)
𝑓∗𝐼𝑜𝑢𝑡𝑚𝑎𝑥∗∆𝐼𝐿%∗𝑉𝑖𝑛𝑚𝑎𝑥 [2] (4)
𝐿𝑏𝑜𝑜𝑠𝑡 >𝑉𝑖𝑛𝑚𝑖𝑛
2 ∗(𝑉𝑜𝑢𝑡−𝑉𝑖𝑛𝑚𝑖𝑛)
𝑓∗𝐼𝑜𝑢𝑡𝑚𝑎𝑥∗∆𝐼𝐿%∗𝑉𝑜𝑢𝑡2 [2] (5)
Industry recommends selecting ∆𝐼𝐿% between 0.2 and 0.4 [2]. In this application ∆𝐼𝐿% was set to 0.3. This value
ensures that the converter doesn’t operate in discontinuous conduction mode, where the current becomes negative.
Equations 2 and 3 provide the critical inductance that meets. Using the specifications above, the inductor value was
chosen to be 50 𝜇H, exceeding the critical inductance value. For high efficiency, the inductor must have low core
loss, low DC resistance losses, and must handle peak inductor current without saturating.
The LT8390 employs a current mode control for constant frequency operation. In current mode control, a inductor
current sense resistor is used to detect and limit the peak inductor current. The sense resistor is chosen based on the
required output current. The duty cycle independent maximum current sense thresholds (50 mV in peak-buck and
50 mV in peak-boost) set the maximum inductor peak current in the buck, buck-boost, and boost regions. The sense
resistor is calculated using equations 4-7.
𝑅𝑠𝑒𝑛𝑠𝑒(𝑏𝑜𝑜𝑠𝑡) =2×50 𝑚𝑉×𝑉𝑖𝑛(𝑚𝑖𝑛)
2×𝐼𝑜𝑢𝑡(max)×𝑉𝑜𝑢𝑡+∆𝐼𝐿(𝑏𝑜𝑜𝑠𝑡)×𝑉𝑖𝑛(min) [2] (6)
𝑅𝑠𝑒𝑛𝑠𝑒(𝑏𝑢𝑐𝑘) =2×50 𝑚𝑉
2×𝐼𝑜𝑢𝑡(max)+∆𝐼𝐿(𝑏𝑢𝑐𝑘) [2] (7)
where,
∆𝐼𝐿(𝑏𝑜𝑜𝑠𝑡) =𝑉𝑖𝑛(𝑚𝑖𝑛)×(𝑉𝑜𝑢𝑡−𝑉𝑖𝑛(𝑚𝑖𝑛))
𝑓𝑠×𝐿×𝑉𝑜𝑢𝑡 [2] (8)
∆𝐼𝐿(𝑏𝑢𝑐𝑘) =𝑉𝑜𝑢𝑡×(𝑉𝑖𝑛(max)−𝑉𝑜𝑢𝑡)
𝑓𝑠×𝐿×𝑉𝑖𝑛(max) [2] (9)
13
The final sense resistor value was chosen to be lower than the calculated sense resistor value in buck and both
region, and low equivalent series inductance (ESL). After selecting an appropriate value for the sense resistor, the
lowest maximum average load current in boost and buck region can be calculated using equations 8 and 9.
𝐼𝑜𝑢𝑡(max _𝑏𝑜𝑜𝑠𝑡) = (50 𝑚𝑉
𝑅𝑠𝑒𝑛𝑠𝑒−
∆𝐼𝐿(𝑏𝑜𝑜𝑠𝑡)
2) ×
𝑉𝑖𝑛(min)
𝑉𝑜𝑢𝑡[2] (10)
𝐼𝑜𝑢𝑡(max _𝑏𝑢𝑐𝑘) = (50 𝑚𝑉
𝑅𝑠𝑒𝑛𝑠𝑒−
∆𝐼𝐿(𝑏𝑢𝑐𝑘)
2) [2] (11)
The LT8390 uses four external n-channel power MOSFETS for the switching scheme. Important parameters for the
power MOSFETS include the breakdown voltage 𝑉𝐵𝑅(𝐷𝑆𝑆), on-resistance 𝑅𝐷𝑆(𝑂𝑁), reverse transfer capacitance 𝐶𝑅𝑆𝑆,
and maximum current 𝐼𝐷𝑆(𝑚𝑎𝑥). To select the power MOSFETS, the power dissipated by the MOSFETS must be
known. The maximum power dissipation for each switch is calculated using equations 10-13.
𝑃𝐴(𝑏𝑜𝑜𝑠𝑡) = (𝐼𝑜𝑢𝑡(max)×𝑉𝑜𝑢𝑡
𝑉𝑖𝑛)2 × 𝜌𝑇 × 𝑅𝐷𝑆(𝑂𝑁) [2] (12)
𝑃𝐵(𝑏𝑢𝑐𝑘) = (𝑉𝑖𝑛−𝑉𝑜𝑢𝑡
𝑉𝑖𝑛) × 𝐼𝑜𝑢𝑡(max)
2 × 𝜌𝑇 × 𝑅𝐷𝑆(𝑂𝑁)[2] (13)
𝑃𝐶(𝑏𝑜𝑜𝑠𝑡) = ((𝑉𝑜𝑢𝑡−𝑉𝑖𝑛)×𝑉𝑜𝑢𝑡
𝑉𝑖𝑛2 ) × 𝐼𝑜𝑢𝑡(max)
2 × 𝜌𝑇 × 𝑅𝐷𝑆(𝑂𝑁) + 𝑘 × 𝑉𝑜𝑢𝑡3 ×
𝐼𝑜𝑢𝑡(max)
𝑉𝑖𝑛× 𝐶𝑅𝑆𝑆 × 𝑓𝑠 [2]
(14)
𝑃𝐷(𝑏𝑜𝑜𝑠𝑡) =𝑉𝑜𝑢𝑡
𝑉𝑖𝑛× 𝐼𝑜𝑢𝑡(max)
2 × 𝜌𝑇 × 𝑅𝐷𝑆(𝑂𝑁) [2]
(15)
The BSZ100N06LS3 G n-channel MOSFET manufactured by Infineon Technologies meets the maximum
breakdown voltage 𝑉𝐵𝑅(𝐷𝑆𝑆) , current 𝐼𝐷𝑆(𝑚𝑎𝑥) and low on-resistance 𝑅𝐷𝑆(𝑂𝑁) which minimizes power losses. Table
I shows the absolute maximum ratings of the MOSFETS. Table I shows the maximum breakdown voltage 𝑉𝐵𝑅(𝐷𝑆𝑆)
for the four switches during simulation. Switches A and B have a maximum breakdown voltage in the buck region,
and switches C and D have a maximum breakdown voltage in the boost region. Table III shows the maximum drain
current and drain pulse current for each switch based on simulation. Using simulation, each switch was analyzed for
the three cases, determining at what cases the switches deliver maximum drain current and drain pulse current.
Absolute Maximum Ratings n-channel MOSFET BSZ100N06LS3 G
Breakdown voltage 𝑉𝐵𝑅(𝐷𝑆𝑆) 60 V
Drain current 𝐼𝐷𝑆(𝑚𝑎𝑥) 20 A
Pulse drain current 𝐼𝐷𝑝𝑢𝑙𝑠𝑒(𝑚𝑎𝑥) 80 A
on-resistance 𝑅𝐷𝑆(𝑂𝑁) 10 mΩ
Reverse transfer capacitance 𝐶𝑅𝑆𝑆 24 pF
Table I: Maximum ratings for the n-channel MOSFET BSZ100N06LS3 G from Infineon Technologies [19].
Switch A Switch B Switch C Switch D
Maximum Voltage
Rating 60V 60V 36V 36V
14
Table II: Maximum voltage ratings for the four external switches based on simulation.
Switch A Switch B Switch C Switch D
Maximum Drain
Current 2.45 A 3.57 A 155.37 mA 6.305 A
Maximum Drain
Pulse Current 77.41 A 73.06 A 22.57 A 18.84 A
Table III: Maximum drain and drain pulse current for the four external switches based on simulation. The drain
pulse currents last no more than 10 nanoseconds.
The Safe Operating Area graph of the BSZ100N06LS3 G n-channel MOSFET displays the power the MOSFET can
handle within a time frame. According to figure V, the MOSFET can handle a maximum pulse power of 4.8 kW for
1 microsecond.
During simulation, all four external switches didn’t exceed this power limit,
Figure V: Safe Operating Area of the n-channel MOSFET BSZ100N06LS3 G. [19]
The Safe Operating Area shows that the MOSFET has a maximum power dissipation of 4.8 kW, maximum drain to
source voltage of 60 V, and maximum permissible drain current of 80 A for a time period of 1 microsecond [19].
Input and output capacitance are necessary to suppress voltage ripple caused by discontinuous current moving in and
out of the regulator. 1 µF ceramic capacitors are placed near the regulator’s input and output to suppress high
frequency switching spikes, and significantly reduce input ripple voltage and power loss.
15
Input capacitance network is sized to handle maximum RMS current with low equivalent series resistance (ESR).
Equation 14 offers a simple worst-case scenario solution commonly used for design, because significant deviations
do not offer much relief.
𝐼𝑟𝑚𝑠 =𝐼𝑜𝑢𝑡(max)
2 (16)
Output capacitance network is sized to reduce the output voltage ripple and low ESR. The effects of ESR and bulk
capacitance must be considered. The output capacitance network is calculated using equations 15 and 16.
𝐶𝑜𝑢𝑡(𝑏𝑜𝑜𝑠𝑡) =𝐼𝑜𝑢𝑡(max)×(𝑉𝑜𝑢𝑡−𝑉𝑖𝑛(min))
𝑉𝑜𝑢𝑡×𝑓𝑠×∆𝑉𝑐𝑎𝑝(𝑏𝑜𝑜𝑠𝑡) [2] (17)
𝐶𝑜𝑢𝑡(𝑏𝑢𝑐𝑘) =𝑉𝑜𝑢𝑡×(1−
𝑉𝑜𝑢𝑡𝑉𝑖𝑛(max)
)
8×𝐿×𝑓𝑠2×∆𝑉𝑐𝑎𝑝(𝑏𝑢𝑐𝑘)
[2] (18)
The final critical output capacitance network is chosen higher than the calculated values in boost and buck region.
Choosing a value high ensures that it meets the output voltage ripple specification.
After component sizing of the inductor, sense resistor, MOSFETs, and input and output capacitance network, the
three corner cases are simulated using LTSpice. The .net file for the simulations can be found in Appendix B.
Corner case 1:
𝑎) 𝑉𝑖𝑛 = 10 𝑉 𝑏𝑜𝑜𝑠𝑡 𝑚𝑜𝑑𝑒
b) 𝑉𝑜𝑢𝑡 = 36 𝑉
c) electronic load = 0.277 A
d) resistive load = 130 Ω
For corner case 1, the input voltage is set to 10 V with two different loads: a current source which acts as an
electronic load, and a resistive load. Simulation of two different loads ensures that the circuit doesn’t alter the user
experience of the elliptical machine. The electronic load is based on assuming 100% efficiency. At 10 V, the
elliptical machine produces 1 A, and thus 10 W. Using the power equation 𝑃 = 𝑉𝑜 × 𝐼𝑜 and an output voltage of 36
V, an 𝐼𝑜 of 0.277 A is calculated and used to validate the corner case works. Using the power equation 𝑃 =𝑉2
𝑅 and
an output voltage of 36 V, a resistive load of 130 Ω is calculated and used to validate the corner case works. At low
load of 10 W, the efficiency decrements, with an efficiency of 54.4%.
16
Figure VI: 36 V output voltage and less than 1 V output voltage ripple with 0.277 An electronic load.
Figure VII: Boost region inductor current waveform using electronic load.
17
Figure VIII: Drain to Source voltage waveforms for four external MOSFET switches using electronic load. As
expected in boost region, switches C and D alternate, switch A is always on, and switch B is always off.
Figure IX: 36 V output voltage and less than 1 V output voltage ripple with 130 Ω resistive load.
18
Figure X: Boost region inductor current waveform using a resistive load.
Figure XI: Drain to Source voltage waveforms for four external MOSFET switches using a resistive load. As
expected in the boost region, switches C and D alternate, switch A is always on, and switch B is always off.
Corner case 2:
𝑎) 𝑉𝑖𝑛 = 60 𝑉 𝑏𝑢𝑐𝑘 𝑚𝑜𝑑𝑒
b) 𝑉𝑜𝑢𝑡 = 36 𝑉
c) electronic load = 5.4 A
d) resistive load = 5.3 Ω
For corner case 2, the input voltage is set to 60 V with two different loads: a current source which acts as an
electronic load, and a resistive load. Simulation of two different loads ensures that the circuit doesn’t alter the user
experience of the elliptical machine. The electronic load is based on assuming 100% efficiency. At 60 V, the
19
elliptical machine produces 6 A. The current source acting as an electronic load is calculated using 𝑃 = 𝐼𝑜 × 𝑉𝑜. At
100 % efficiency, the elliptical machine delivers 360 W. Using a power of 360 W and 𝑉𝑜 of 36 V, a current source of
10 A is calculated. However, after several simulation attempts, 5.4 A is the maximum current load the controller
provides. Using 𝑃 =𝑉𝑜
2
𝑅 , P of 360 W, and 𝑉𝑜 of 36 V, a resistive load of 3.6 Ω is calculated. However, after several
simulation attempts, the minimum resistive load the controller works with is 5.3 Ω. At high loads, the efficiency
increases to 92.9%.
Figure XII: 36 V output voltage and less than 1 V output voltage ripple with 5.4 An electronic load.
Figure XIII: Buck region inductor current waveform using electronic load.
20
Figure XIV: Drain to Source voltage waveforms for the four external MOSFET switches using an electronic load.
As expected in the buck region, switches A and B alternate, switch D is always on, and switch C is always off.
Figure XV: 35.61 V output voltage and less than 1 V output voltage ripple with 5.3 Ω resistive load.
21
Figure XVI: Buck region inductor current waveform using a resistive load.
Figure XVII: Drain to Source voltage waveforms for the four external MOSFET switches using a resistive load. As
expected in the buck region, switches A and B alternate, switch D is always on, and switch C is always off.
22
Corner case 3:
𝑎) 𝑉𝑖𝑛 = 37 𝑉 𝑏𝑢𝑐𝑘 𝑏𝑜𝑜𝑠𝑡 𝑚𝑜𝑑𝑒
b) 𝑉𝑜𝑢𝑡 = 36 𝑉
c) electronic load = 3.7 A
d) resistive load = 10 Ω
For corner case 3, the input voltage is set to 37 V with two different loads: a current source which acts as an
electronic load, and a resistive load. Simulation of two different loads ensures that the circuit doesn’t alter the user
experience of the elliptical machine. The electronic load is assuming a current-voltage linear relationship. At 10 V
the elliptical machine produces 1 A, and at 60 V the elliptical machine produces 6 A, therefore, for an input voltage
of 37 V, it is assumed the elliptical machine produces 3.7 A. Efficiency is assumed 100%. Using the power equation
𝑃 =𝑉2
𝑅 , P of 137 W, and an output voltage of 36 V, a resistive load of 10 Ω calculated. Efficiency slightly
decreased to 91.9%.
Figure XVIII: 36.19 V output voltage and less than 1 V output voltage ripple with 3.7 An electronic load.
23
Figure XIX: Buck-boost region inductor current waveform using an electronic load.
Figure XX: Drain to Source voltage waveforms for the four external MOSFET switches using an electronic load.
As expected in the buck-boost region, all switches alternate at different duty cycles. Switch C has a duty cycle of
approximately 15% and switch D has a duty cycle of approximately 85%.
24
Figure XXI: 36.19 V output voltage and less than 1 V output voltage ripple with 10 Ω resistive load.
Figure XXII: Buck-boost region inductor current waveform using a resistive load.
25
Figure XXIII: Drain to Source voltage waveforms for the four external MOSFET switches using a resistive load.
As expected in the buck-boost region, all switches alternate at different duty cycles. Switch C has a duty cycle of
approximately 15% and switch D has a duty cycle of approximately 85%.
After successful simulations for the corner cases and rigorous component sizing calculations, the next step is the
PCB layout consideration. The next chapter documents the PCB layout design, including component layout choices,
and struggles faced during the process.
26
Chapter 6: Component Selection and PCB Layout
This section walks through the selection of the components and the criterion it was based upon. Following the
component selection, the process of laying out the board is documented along with the design considerations. The
board design and layout are done using KiCad. KiCad is being because it is free, open-source, and easy to use.
The first components selected were the power MOSFETs necessary for providing the switching capabilities. Due to
the input voltage range varying from 5-60 volts, the input MOSFETS need a VDS breakdown voltage of at least 60
V. With the output voltage at a constant 36 V, the output MOSFETS need a VDS breakdown voltage of at least 36 V.
The max current seen is 8 A, so the MOSFETS need to be able to handle this. The component values need to include
a safety margin if a circuit failure occurs. The Infineon power series BSZ100N06LS3 NMOSFET provided a great
solution and met the specifications required. This MOSFET was provided in the LTSpice test bench for the LT 8390
and no other MOSFETs were considered because these fully met the specifications. Table VI shows the necessary
specifications for the NMOSFET.
Table VI
BSZ100N06LS3 NMOS Specifications [19]
Specification BSZ100N06LS3
VDS Breakdown Voltage 60 V
Current Rating 20 A
RDS On 10 mΩ
Input Capacitance 2.6 nF
Max Power Dissipation 50 W
In order for the microinverter to efficiently handle the output voltage of the converter, the output voltage ripple must
be reduced to a minimum. The specifications in table I define an output voltage ripple of 1.8 volts. After the first
iteration, seen in figure V, the output ripple extremely exceeded this value. To reduce this, a large 620 𝜇F capacitor
was introduced to the output voltage node. This value was arbitrarily chosen as a starting point to tweak the output
capacitance. This largely decreased the output ripple seen in the simulations. One concern was the total equivalent
series resistance of the capacitors. If the ESR were to be too high, it causes high losses in the capacitor along with
additional unwanted ripple. Upon learning the efficiency of the converter was lower than anticipated, about 84%, the
output capacitance is reduced. This could be done because the output ripple specification had some room to change.
The efficiency of the converter rose to meet our specification, about 96%.
Other design considerations to keep in mind were the package footprint, frequency ratings, cost, and availability, but
these design considerations required less thought as those mentioned above. Figure XXIV shows the schematic for
the first revision. Table V shows the preliminary estimate for costs.
27
Figure XXIV: Schematic for First Revision of Board
28
The LT8390 datasheet provides valuable information and important considerations for laying out the PCB. Some of
the more notable examples include, placing switch A and the input capacitance, and switch B and the output
capacitance as close to the IC as possible, placing the negative terminals of the capacitors as close as possible, and
using planes for Vin and Vout. To manufacture the PCB, expressPCB and their MiniBoardPlus Service is used. This
service sets out certain footprint of 3.8 x 2.5 inches which puts constrains on the number of components and the real
estate to layout the components on the board. The first revision of the board is seen in figures XXV and XXVI.
Figure XXV: Front Layer for First Revision of Board
29
Figure XXVI: Back Layer for First Revision of Board
30
Some struggles first encountered when laying out this board were the large amount of considerations to keep in
mind. Keeping the board organized while also trying to pay attention to important nuances took a large amount of
time. Once all the components were in a reasonable configuration is was time to route all the nets to their
connections. Thanks to auto-routing tool, the traces were made. Once the auto-routing tool was completed, a couple
modifications had to be made. The first modification was the minimum trace width needed for the ground plane. The
minimum trace width was too large which didn’t allow the GND pin, which was near the other pins, to be connected
to the ground pour. The minimum trace width was reduced which remedied the issue. The other modification needed
was due to some isolated ground pours not connecting on the front layer. Vias were used to connect these ground
pours together. Other slight changes were made, such as small route changes and small components movements to
give more room for the traces.
Upon reviewing the first revision, multiple aspects on the board required attention. First, the board had no access to
reach the outside world. Three, four millimeter, holes are added allowing banana plug terminals to be screwed
through the board. One for Vin, Vout, and GND. Many of the components also had no way of dissipating heat, so
the critical power components had several thermal vias added. Finally, the power lines were given wider trace
widths to permit the high current seen in the switching modes of the converter. These changes are seen in figures
XXVII through XXIX.
31
Figure XXVII: Schematic for Second Revision of Board
32
Figure XXVIII: Front Layer for Second Revision of Board
33
Figure XXIV: Back Layer for Second Revision of Board
34
After discussions with Professor Braun and reviewing the second revision of the board, several major issues were
found. The main issue with both revisions of the board was the lack of power planes for many of the nets. The traces
defined for the power paths would not handle the high current. Power planes were added for the Vin, SW1, LSN,
SW2, Vo, and Vout nets to handle the large amount of current, and thus power. The power path follows the direction
seen by the black arrows in figure XXXIV. The digital signals, which produce far lower currents, are found in the
middle of the board closest to the IC. Two separate ground planes were created allowing the signals to return to the
correct plane from which it was originated. Thermal vias were added to the bottom of the IC to prevent overheating.
Vin and Vout both needed separate ground plugs, so another plug was added. No new components were added, so
refer to figure XXVIII for schematic.
Figure XXXI: Front Layer for Third Revision of Board
35
Figure XXXII: Back Layer for Third Revision of Board
36
Small, quality-of-life, changes were made to the third revision to complete the board. The digital plane was shrunk
to shorten the return path for digital signals. A new inductor was switched out for the previous chosen one, so a new
footprint was created to accommodate this change. Paths that had originally thought to handle low currents were
increased due to their actually high current loads. Finally, test points were added to the gates of each transistor and
on opposites sides of the sense resistors for troubleshooting purposes.
37
Figure XXXIII: Schematic for Final Revision of Board
38
Figure XXXIV: Front Layer for Final Revision of Board
39
Figure XXXV: Back Layer for Third Revision of Board
40
OSH Park was used as the fab house for this design. They provide an easy to use interface for uploading designs and
cost-effective boards. The next chapter outlines the assembly of the PCB’s and the issues faced during this process.
41
Chapter 7: Assembly
After receiving the PCB’s from OSH Park, the assembly process started. The lack of a solder stencil required hand
soldering for all the components. This required precise soldering for the IC and the MOSFETs. Using the Hakko
FX-888D the soldering portion of the process begun. To expedite the process and keep the components stationary on
the board when soldering, one pad for each resistor and capacitor was tinned. Flux is applied before tinning for a
cleaner solder joint. After each component had one side soldered to the board, the IC was next to be soldered. The
IC has very small pads, so the ground pad underneath the IC was tinned and then reheated, which allowed the IC to
fall into place. This kept it in place, so the IC would not move when soldering the other pads. After carefully
soldering the pads of the IC, the MOSFETs were next. The same process was followed to secure and solder the
MOSFETs to the board. Lastly, the inductor is soldered to the board. Due to an error in the board layout, external
wires are needed to connect the inductor. 18-gauge wires are used to handle the, up to six amps, current seen through
the inductor. The final soldered board is seen in figure XXXVI. The next chapter will outline the testing procedure.
Figure XXXVI: Final soldered PCB
42
Chapter 8: DC-DC Converter Testing
This chapter documents the steps and procedures for converter testing. Testing involves using an electronic load to
ensure the converter functions as expected.
Figure XXXVII: Test setup for DC-DC Converter.
The converter initially tests low loads to prevent overheating or component damage. At high loads, the converter
sees higher currents, which could possibly damage components. The BK Precision DC 8540 electronic load is set
initially at 1 A and increased to 4 A in steps of 1 A. Using the RIGOL DP832 DC power supply the input voltage is
initially set at 10 V and increased to 60 V in steps of 5 V. This ensures enough data points for validation. For each
load, the input voltage ranges from 10-60 V. This procedure allows us to determine the efficiency of the converter at
different loads.
The load and line regulation describe performance parameters of the converter that analyze converter performance.
The load regulation indicates how well the converter sustains a constant output voltage at different loads. The line
regulation indicates how well the converter sustains a constant output voltage at different input voltages. Equations 1
and 2 calculate the load and line regulation, and equation 3 calculates efficiency/
𝑙𝑜𝑎𝑑 𝑟𝑒𝑔𝑢𝑙𝑎𝑡𝑖𝑜𝑛 % = 𝑉𝑜𝑁𝑜 𝐿𝑜𝑎𝑑−𝑉𝑜𝐹𝑢𝑙𝑙 𝐿𝑜𝑎𝑑
𝑉𝑜𝐹𝑢𝑙𝑙 𝐿𝑜𝑎𝑑× 100 (1)
𝑙𝑖𝑛𝑒 𝑟𝑒𝑔𝑢𝑙𝑎𝑡𝑖𝑜𝑛 % = 𝑉𝑜𝐿𝑜𝑤 𝑖𝑛𝑝𝑢𝑡 𝑣𝑜𝑙𝑡𝑎𝑔𝑒−𝑉𝑜𝐻𝑖𝑔ℎ 𝑖𝑛𝑝𝑢𝑡 𝑣𝑜𝑙𝑡𝑎𝑔𝑒
𝑉𝑜𝑁𝑜𝑚𝑖𝑛𝑠𝑙 𝑖𝑛𝑝𝑢𝑡 𝑣𝑜𝑙𝑡𝑎𝑔𝑒× 100 (2)
𝑒𝑓𝑓𝑖𝑐𝑖𝑒𝑛𝑐𝑦 % = 𝑃𝑜𝑢𝑡
𝑃𝑖𝑛× 100 (3)
The next chapter will describe the future plans for the product and the major lessons learned.
43
Chapter 9: Future Plans and Takeaways
At the end of this project, many things need extra research and further iterations to have a fully-fledged out design.
The process also provided many opportunities to learn from that will help guide us through our career in the future.
The main setback in this project is the limited time to design, manufacture and test the PCB. Plans to create a second
revision of the PCB are in the works that would reduce clutter on the board. Thermal vias for the MOSFETs are also
planned to be added to increase the efficiency of the heat dissipated by the MOSFETs. Allowing more room for
extra caps on the feedback, output, and input nets would create an opportunity to add more caps without having to
fabricate a whole new board. Most importantly the footprint of the inductor could be correctly mapped out,
completely reducing the need for external wires.
More research into other IC’s and different values for resistors and capacitors would give rise to a possible increase
in efficiency, cheaper BOM, or better performance in regard to our design specifications. The project was based
around the use of the LT 8390 without much research into other IC’s, so looking at other ones might uncover a
better performing converter. Tests including the elliptical machines would be valuable data to capture as well.
Rather than using a DC power supply to generate the input voltage, the elliptical machine would provide this
voltage. This testing would really put the design to the test for the desired application and see how well the
simulations matched up the real-life conditions.
The most important plans for the project would be further testing of the current iteration. We ran out of time to
further test and debug the circuit, which stopped us from finding the reason that the circuit was not performing to
our standards. This situation caused no verifiable and quality data to be collected, and, in the end, no confirmation if
the circuit that was designed worked as designed.
The main takeaway from this project, which really delayed our project in the end, was the significant amount of time
simulation and PCB layout took. The simulation phase, one of the most critical phases, took considerable time to
produce the results that were laid out in the design specifications. The effect of changing one component had a
cascading effect on other components which made slight changes turn into large shifts in the output. After many
iterations, a design that we were confident with was chosen. The PCB design process followed suit. The datasheet
had many considerations to keep in mind, which are there not as suggestions, but rather informing you that the
project will not work as intended if they were not followed. The process also took a considerable amount of time,
longer than we had anticipated. Having little experience in designing power-based boards really slowed down the
progress. More than three major iterations were done, with many minor iterations in between. If this process were to
be done again, more time would be allotted to these two phases.
Some other takeaways that really made an impact were the manufacturing lead times and importance of preliminary
work. A major time delay was due to the time it took from when we ordered the components and PCB to when we
received them. This delayed the project at least a week and half where we couldn’t do any physical testing. This
delay put the project to the final days and put a considerable time pressure on us. The design work done in EE 460
set up a fantastic foundation for the design phase of the project. Having very specific and measurable design
requirements really allowed the design to have no wiggle room in terms of the output and desirable metrics.
44
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[17] IEEE. IEEE Std 1233, 1998 Edition, p. 4 (10/36), DOI: 10.1109/IEEESTD.1998.88826
[18] United States Department of Energy. “2017 U.S. Energy and Employment Report.” Department of Energy,
www.energy.gov/downloads/2017-us-energy-and-employment-report.
45
[19] Author, Unknown. “Infineon BSZ100N06LS3 Data Sheet.” Infineon BSZ100N06LS3 Data Sheet, 2009,
www.infineon.com/dgdl/Infineon-BSZ100N06LS3-DS-v02_03-
en.pdf?fileId=db3a30431ddc9372011ebb132c97000a.
[20] R. Morgan, "What Is the Average Gross Profit Margin for a Small Retail Business?", Smallbusiness.chron.com,
2018. [Online]. Available: http://smallbusiness.chron.com/average-gross-profit-margin-small-retail-
business-22607.html. [Accessed: 20- Feb- 2018].
[21] A. Sireci, "DC-DC Converter Control System for the Energy Harvesting from Exercise Machines System",
2017. [Online]. Available:
http://digitalcommons.calpoly.edu/cgi/viewcontent.cgi?article=3014&context=theses. [Accessed: 27- Feb-
2018].
[22] Y. Benitez Ramirez, J. Gonzalez Herrera and J. Rosero Garcia, "Technical evaluation of the electric energy
production process within a distributed generation model for gyms in Colombia", 2012 IEEE International
Symposium on Alternative Energies and Energy Quality (SIFAE), 2012.
[23] T. Gibson, "Turning sweat into watts", IEEE Spectrum, vol. 48, no. 7, pp. 50-55, 2011.
[24] U. Author. Strength Companion LLC, "Energy harvester for exercise equipment", US8888660B1, 2011.
46
Appendix A - Analysis of Senior Project Design
Project Title: Energy Harvesting from Exercise Machines
Student’s Name: Alexander Samietz Student’s Signature: Alexander Samietz
Gustavo Guzman Gustavo Guzman
Advisor’s Name: David Braun Advisor’s Initials: D.B. Date: March 3, 2018
1. Summary of Functional Requirements
This project provides a high efficiency DC-DC buck-boost converter using the LT8390 controller for energy
harvesting. The project harvests unused energy produced by an elliptical machine and delivers power back to the
electrical grid. The project applies to the Recreational Center at Cal Poly.
2. Primary Constraints
When referencing the requirements and specifications back in chapter 2, the project could run into issues trying to
accomplish them. For example, the elliptical could generate 5-60 volts due to variable workout intensities and
variable strides-per-minute (SPM). The solution to the problem uses a controller that accepts the large voltage range
and efficiently converts it to a proper output voltage required to safely deliver energy to the grid. Testing ensures
variable component tolerances meet outlined specifications. The product’s lifetime adds another constraint. The
converter’s lifetime depends on the elliptical machine. Having the converter’s lifetime shorter than the elliptical
machine’s lifetime would result in an inefficient product.
3. Economic
Human Capital: The project doesn’t seem to have an enormous effect on human capital, however a deeper
investigation exposes more than what meets the eye. For example, selling large units, on the order of thousands to
hundreds of thousands, of the energy harvesting elliptical machine could decrease power plant jobs. However,
selling large units of the machine that affect power plant job growth forms an extreme case, but it remains a
possibility.
Financial Capital: Financial capital marks one of two categories where the project would have most impact. Think of
the project like investing in solar panels. It requires a large upfront investment without immediate investment return,
but once surpassing the breakeven point, investment returns increase. The elliptical and converter cost an initial
investment, but over the products lifetime course, the investment returns more financial capital. The project
decreases monthly energy costs.
Manufactured or Real Capital: Component and controller manufacturing see a production increase due project
purchases. A potential partnership with an exercise machine manufacturer stems an enticing project aspect. For
example, if only Precor elliptical machines came with an energy harvester it could bring a boost in production for
their brand of elliptical machines, while reducing the production of others. This could create fascinating real capital
considerations, and something to explore further in both manufactured and financial capital.
Natural Capital: Due to today's increasing energy needs, one's ability to create their own energy adds value. This
reduces grid strains and power plant energy production, thus reducing environmental impacts. Also, creating a
sustainable product and having the user see its environmental impact, has the possibility for the user to live a more
sustainable lifestyle.
47
The costs almost equal initial investment, but once the energy harvested overtakes initial device cost, the benefits
outgrow the initial investment.
The project requires any gym goer to use the device which initiates energy harvesting. Production costs shouldn’t
exceed $360. This number stems from conservative estimates of 100W workout, with 90% inverter efficiency, 80%
DC-DC converter efficiency, and 12 hours of machine use per day for 41 weeks per year [1]. Product consumers
make up of gym enthusiast and owners, specifically Cal Poly Rec Center.
With estimated 150 work project hours at $47.41 hourly rate, the labor approximates at $7,156. A starting engineer’s
hourly rate shoots close to $47.41 according to the bureau of labor statistics [16]. This price fluctuates and may
change. The actual project work hours came to 198 hours giving a total of 9,387.18. An additional elliptical machine
used for previous projects provides testing purposes.
Depending on usage amount and project life cycle, the project can produce variable amounts of money. Determining
the products overall revenue without a finished product to analyze. The breakeven point mentioned above, of about
$350, seems like a reasonable educated guess [1].
The product stands in testing phase, ensuing an unknown production timeline. More testing ensures product
reliability, environmental responsibility, and efficiency. The product should not affect elliptical machine
performance and should last the elliptical machine’s lifetime. Proper converter construction and designing requires
minimal maintenance.
The estimated time follows:
Time Optimistic = To = 100
Time Most Likely = Tm = 150
Time Pessimistic = Tp = 200
𝐸𝑥𝑝𝑒𝑐𝑡𝑒𝑑 𝑇𝑖𝑚𝑒 =𝑇𝑜 + 4𝑇𝑚 + 𝑇𝑝
6=
100 + 600 + 200
6= 150 ℎ𝑜𝑢𝑟𝑠
Once the project ends, two options emerge:
1. If nearly completed, production and manufacturing can start.
2. If unfinished, the project needs more testing and design revisions.
4. If manufactured on a commercial basis:
Because of the twenty elliptical machines in the Cal Poly REC center, it estimates twenty product manufacturing
units for the first year. The device manufacturing cost would follow the estimate mentioned of about $350 per
device, not including the elliptical machines. Selling the device for $500 would result in a price margin of 30%. This
price margin mimics other products sold, which normally run a profit margin of 25%-50% [2]. If an elliptical
machine runs for ten years before replacement, then the cost per unit time reaches fifty dollars per year.
5. Environmental
The project connects to the electrical grid. Natural resources build and run the electrical grid. The project indirectly
requires natural grid power resources like coal, natural gas, fossil fuels, wind, nuclear, hydro and thermal sources. In
start of harvesting coal, fossil fuels, and natural gas, species inhibiting the land forcibly evacuate and relocate, which
possibly affects their ecosystem. Electronics create byproducts after their lifetime. If disposed inappropriately, the
byproducts release harmful, environmental chemicals. Harming the environment directly affects humans and other
species. Manufacturing and PCB fabrication use natural resources like silicon and copper.
48
6. Manufacturability
A few manufacturing issues include metal trace tolerances when fabricating the PCB. Considering the tolerances
ensures unintended PCB issues arise. If the generated heat from the controller is improperly handled, issues could
arise where parts either perform unacceptably or entirely burned. PCB layout factors an important part in
manufacturability. Part placement ensures product functions at maximum capacity, by reducing chip space and
board size. Minimizing wire usage guarantees less noise and clean waveforms during testing.
7. Sustainability
The device’s purpose creates a sustainable approach in using the gym. Users can use this device knowing they
contribute in a greener, more sustainable future by help powering the gym. A design improvement consideration,
which may not make it more sustainable per se, would display the user’s harvested energy. This would not only
encourage machine usage and preference over others, and show positive environmental impacts the user develops.
By directly seeing the feasibility for a decrease in energy footprint per person, this could also influence the user to
live a more sustainable life outside of the gym. For example, this person could ride their bike to work, or purchase
local foods to reduce their environmental footprint.
8. Ethical
Ethical principlism surrounds the ethical framework behind the project. In autonomy terms, the product does not
force the user product preferences over another. Choosing a product that doesn’t harvest energy results as an
individual choice. Regards to non-maleficence, the product has no harmful intentions to those using it. Imagine a
situation where a person forces another person to use the machine against their willpower to save money. This
would go against the do-no harm value and affect the autonomy of the one using it. This product also follows the
beneficence principle. The product reduces environmental harm by taking wasteful energy and converting it to
useful energy. Lastly, the principle of justice applies that people have the freedom to live a healthy life, so those
wanting to contribute a sustainable lifestyle should have that freedom of choice.
IEEE also lays out a code of ethics that members must follow. Some IEEE guidelines have higher implications than
others regarding the product. For example, honesty and realistic claims that the product functions as properly
marketed. The product should produce energy as described and in no way should state any falsehoods. Another
guideline accepts the criticism of the work done. If the product has criticisms, it’s important to acknowledge them
and then promptly address them. The last guideline addresses avoiding injury to others, their property, or reputation.
The device production, in no way, should have any intended negative uses. It should only provide user benefits. If
not the case, any mistakes are immediately and responsibly handled.
9. Health and Safety
Delivering unused energy back to the grid stems a health and safety concern. However, following the UL and IEEE
guidelines and standards ensures safety and cautionary protocols. Also, the project requires physical activity, so the
operation of the elliptical machine imposes a safety risk for the user. The user could fall or tangle themselves in the
rotation of the machine and cause harm to themselves or potentially others. The projects goal reuses dissipated heat
from exercising machines and the person operating the machine requires a performance level above average to
maximize the project’s functionality. The machine does encourage a healthy lifestyle by not only providing a means
of exercise and stress relieve, but it can also encourage a more sustainable life style as well.
10. Social and Political
This product impacts the social and political issues regarding the environment and sustainability. Those who support
the fossil fuel industry and reject climate change find the product useless, because of and unnecessary sustainability,
according to those in favoring the fossil fuel industry. If one gym implemented the product this could cause gym-
goers to choose the sustainable gym, which would affect the sustainable gym’s revenue. It could also cause someone
to not choose a gym because they use this product.
49
The main stakeholder in this project is the Cal Poly Rec center. The direct impact it receives is the reduction of
energy costs and byproduct emissions. On the other hand, the indirect impact is the possibility of more students, or
even residents of San Luis Obispo, visiting the gym which could provide more income. This could cause more
congestion in the gym though, which would cause frustration on those in the gym. The project produces an inequity
in the usage of certain elliptical machines, as ones with this device are used more than others causing a shortage of
usable elliptical machines.
Another stakeholder is those in the surrounding environment. This product reduces the pollution in the atmosphere
by replacing power plant generated energy with that of that produced by the elliptical. This replacing of energy
provides a healthier environment for those living there. Billions of people around the world are inadvertently
affected by how this product is developed, manufactured, and used. Seeing firsthand, the impact of pollution on the
environment it’s important to keep this in mind. If the trend of sustainability continues, in the limit there would be
no need for coal or fossil fuel related power plants. The indirect impact would be loss of jobs and industry in the
power generation sector. Over three million Americans work in this sector and many of them would be out of a job
with training that may no longer be needed. [18]
11. Development
Learning about the Monte Carlo technique introduced a new strategy that shows how component tolerances can
severely affect the desired device output. The Gantt chart demonstrates a fantastic method that lays the project
planning in an organized visual fashion. The literature search, in the references section, assisted in finding reliable,
credible sources that back claims in the report. Anticipated learning outcomes include knowing how to effectively
simulate a circuit, efficiently design a prototype, and build and test the product in the power sector.
50
Appendix B: LTSpice Net File
This describes the .net file for the LTSpice simulation used to verify the designs.
*
C1 N011 0 47nF
C2 N012 0 4.7n Rser=27K Cpar=100p
V1 IN 0 60
R1 SW1 N001 2m
C3 N002 SW1 0.1µ V=100 Irms=2.1 Rser=0.0606238 Lser=0 mfg="KEMET" pn="C1210C104K1RAC"
type="X7R"
M§Q1 IN TG1 SW1 SW1 BSZ100N06LS3
M§Q2 SW1 N004 0 0 BSZ100N06LS3
R2 Vdq3 OUT 15m
C4 Vdq3 0 4.7µ V=50 Irms=15 Rser=0.00481132 Lser=0 mfg="KEMET" pn="C1210C475K5RAC" type="X7R"
C5 SW2 N003 0.1µ V=100 Irms=2.1 Rser=0.0606238 Lser=0 mfg="KEMET" pn="C1210C104K1RAC"
type="X7R"
R3 N013 0 309k
C6 N007 0 4.7µ V=6.3 Irms=0 Rser=0.003 Lser=0 mfg="TDK" pn="C2012X5ROJ475M" type="X5R"
C7 N010 0 0.47µ V=10 Irms=1.32 Rser=0.0460968 Lser=0 mfg="KEMET" pn="C1206C474K8RAC" type="X7R"
XU1 N004 N002 SW1 TG1 SW1 N001 IN N007 N006 MP_01 N010 N010 N010 Vdq3 OUT 0 N008 N011 N009
N012 N013 0 0 Vdq3 TG2 SW2 N003 N005 0 LT8390
R7 N009 0 3.24k tol=1 pwr=0.1
R8 N008 N007 100K
R9 N006 0 165K
R10 IN N006 383K
C9 Vdq3 0 1µ V=50 Irms=0 Rser=0.008 Lser=0 mfg="TDK" pn="C3225X7RlHlO5M" type="X7R"
C10 IN 0 15µ V=63 Irms=2.65653 Rser=22.1 Lser=0
C11 IN 0 4.7µ V=50 Irms=15 Rser=0.00481132 Lser=0 mfg="KEMET" pn="C1210C475K5RAC" type="X7R"
C12 Vdq3 0 4.7µ V=50 Irms=15 Rser=0.00481132 Lser=0 mfg="KEMET" pn="C1210C475K5RAC" type="X7R"
C13 IN 0 1µ V=50 Irms=0 Rser=0.008 Lser=0 mfg="TDK" pn="C3225X7RlHlO5M" type="X7R"
M§Q4 SW2 N005 0 0 BSZ100N06LS3
M§Q3 Vdq3 TG2 SW2 SW2 BSZ100N06LS3
R4 OUT N009 113k tol=1 pwr=0.1
I1 OUT 0 5.4
C14 OUT 0 4.7µ V=50 Irms=4.89 Rser=0.0139203 Lser=0 mfg="KEMET" pn="C1206C475K5PAC" type="X5R"
C15 OUT 0 4.7µ V=50 Irms=4.89 Rser=0.0139203 Lser=0 mfg="KEMET" pn="C1206C475K5PAC" type="X5R"
C16 OUT 0 4.7µ V=50 Irms=4.89 Rser=0.0139203 Lser=0 mfg="KEMET" pn="C1206C475K5PAC" type="X5R"
C17 OUT 0 4.7µ V=50 Irms=4.89 Rser=0.0139203 Lser=0 mfg="KEMET" pn="C1206C475K5PAC" type="X5R"
L1 N001 SW2 47µ Ipk=18.6 Rser=0.0028 Rpar=4427.4 Cpar=0 mfg="Coilcraft" pn="AGP4233-473"
C8 OUT 0 330µ V=63 Irms=1.42 Rser=0.049 Lser=0 mfg="Nichicon" pn="UPL1J331MRH" type="Al electrolytic"
.model NMOS NMOS
.model PMOS PMOS
.lib C:\Users\gusgu\Documents\LTspiceXVII\lib\cmp\standard.mos
.tran 30m startup
.meas Pin AVG -V(IN)*I(V1)
.meas Pout AVG V(OUT)*I(I1)
.meas Eff param Pout/Pin
;step param Iload 1 6 1
* suppress high freq \nswitching spikes
* suppress high freq \nswitching spikes
* X5R dielectrics
* X5R dielectrics
* BSC034N03lS can't handle \n36 V, look into other mosfets with low Rdson
* For resistive load, BS100N06LS3\npass 80 A current pulse, surpassing \nmosfets drain pulse current max of 80A.
* Ceramic caps should be placed\nnear regulator input & output to suppress\nhigh freq, switching spikes.
51
* Cin network should have low \nenough ESR and is sized to handle\nmax rms current.
* Cin has I rms max of 3.5 A.
* Cout network should \nreduce output voltage ripple.
* Cout = 620u
* C = 120u
* C1=50n
* The input and output should have a combination of electrolytic\n and ceramic capacitors for effective noise
filtering and to \nreduce ESR for minimum power loss.
* RT, the frequency setting resistor, should \nbe placed close to the chip.
* To prevent ringing, add a small gate resistance to each MOSFET.
* Always choose a low ESL current sense resistor
* R4 = 84.5k
* R7 = 2.37k
* Changes made for update revisions:\n- changed the feedback resistor dividor network\n- included actual
component parameters for output and input capacitors, inductors\n \nstill need to include actual component
parameters for the noise filtering ceramic caps, so verify all caps
* ouput currernt limit or inductor current limit might be \nthe reason why loads above 5.4 A don't work.
.lib LT8390.sub
.backanno
.end
*